TECHNICAL REPORT Incident of aircraft Airbus A-340
**** Hidden Message ***** TECHNICAL<BR>REPORT<BR>IN-062/2002<BR>Incident of aircraft<BR>Airbus A-340<BR>registration EC-IDF,<BR>at Madrid-Barajas<BR>Airport (Madrid) on<BR>7 September 2002<BR>Technical report<BR>IN-062/2002<BR>Incident of aircraft Airbus A-340 registration<BR>EC-IDF, at Madrid-Barajas Airport (Madrid)<BR>on 7 September 2002<BR>MINISTERIO<BR>DE FOMENTO<BR>SUBSECRETARÍA<BR>COMISIÓN DE INVESTIGACIÓN<BR>DE ACCIDENTES E INCIDENTES<BR>DE AVIACIÓN CIVIL<BR>Edita: Centro de Publicaciones<BR>Secretaría General Técnica<BR>Ministerio de Fomento ©<BR>NIPO: 161-03-011-0<BR>Depósito legal: M. 23.129-2003<BR>Imprime: Centro de Publicaciones<BR>Diseño cubierta: Carmen G. Ayala<BR>COMISIÓN DE INVESTIGACIÓN DE ACCIDENTES E INCIDENTES DE AVIACIÓN CIVIL<BR>Tel.: +34 91 597 89 60 E-mail: <A href="mailto:ciaiac@mfom.es">ciaiac@mfom.es</A> C/ Fruela, 6<BR>Fax: +34 91 463 55 35 <A href="http://www.mfom.es/ciaiac">http://www.mfom.es/ciaiac</A> 28011 Madrid (España)<BR>Foreword<BR>This report is a technical document that reflects the point of view of the Civil<BR>Aviation Accident and Incident Investigation Commission (CIAIAC) regarding<BR>the circumstances in which happened the event being investigated, with its<BR>causes and its consequences.<BR>In accordance with the provisions of Law 21/2003 and Annex 13 to the Convention<BR>on International Civil Aviation, the investigation has exclusively a<BR>technical nature, without having been targeted at the declaration or assignment<BR>of blame or liability. The investigation has been carried out without<BR>having necessarily used legal evidence procedures and with no other basic<BR>aim than preventing future accidents.<BR>Consequently, any use of this report for purposes other than that of preventing<BR>future accidents may lead to erroneous conclusions or interpretations.<BR>This report has originally been issued in Spanish language. This English translation<BR>is provided for information purposes only.<BR>v<BR>Technical report IN-062/2002<BR>T a b l e o f c o n t e n t s<BR>Abbreviations ............................................................................................................................... vii<BR>Synopsis ........................................................................................................................................ ix<BR>1. Factual information ............................................................................................................... 1<BR>1.1. History of the flight ........................................................................................................ 1<BR>1.1.1. Flight Madrid-Tenerife Norte ............................................................................. 1<BR>1.1.2. Stop in Tenerife Norte ....................................................................................... 3<BR>1.1.3. Flight Tenerife Norte-Madrid ............................................................................. 4<BR>1.1.4. Actions taken after landing and evacuation of the passengers ......................... 5<BR>1.2. Injuries to persons .......................................................................................................... 7<BR>1.3. Damage to aircraft ......................................................................................................... 7<BR>1.4. Other damage ................................................................................................................ 7<BR>1.5. Personnel information .................................................................................................... 8<BR>1.5.1. Pilot in command .............................................................................................. 8<BR>1.5.2. Copilot .............................................................................................................. 8<BR>1.5.3. Type rating training ........................................................................................... 9<BR>1.6. Aircraft information ........................................................................................................ 9<BR>1.6.1. Airframe ............................................................................................................ 9<BR>1.6.2. Description of the brake system of the A-340-313 ........................................... 10<BR>1.6.3. Abnormal and emergency procedures related to the brake system .................. 18<BR>1.6.4. Previous maintenance on the aircraft ................................................................ 20<BR>1.6.5. Previous incidences in the brake system of aircraft EC-IDF ............................... 20<BR>1.7. Meteorological information ............................................................................................ 24<BR>1.8. Aids to navigation .......................................................................................................... 24<BR>1.9. Communications ............................................................................................................ 25<BR>1.10. Aerodrome information .................................................................................................. 25<BR>1.10.1. Airport of Tenerife Norte ................................................................................ 25<BR>1.10.2. Airport of Madrid-Barajas ................................................................................ 25<BR>1.11. Flight recorders .............................................................................................................. 25<BR>1.11.1. Cockpit voice recorder .................................................................................... 25<BR>1.11.2. Flight data recorder ......................................................................................... 26<BR>1.12. Wreckage and impact information ................................................................................. 26<BR>1.13. Medical and pathological information ............................................................................ 28<BR>1.14. Fire ................................................................................................................................ 29<BR>1.15. Survival ........................................................................................................................... 29<BR>1.16. Tests and research ......................................................................................................... 29<BR>1.16.1. Ground test to locate the problem ................................................................. 29<BR>1.16.2. Release to service of the aircraft ..................................................................... 30<BR>1.16.3. Inspection of the master cylinder S/N H2121 .................................................. 31<BR>1.16.4. Inspection of the dual valve (BDDV) S/N H2718 ............................................. 33<BR>1.16.5. Additional testing of the master cylinder S/N H2121 ...................................... 33<BR>1.16.6. Inspection of the pedal cover .......................................................................... 33<BR>1.17. Organizational and management information ................................................................ 34<BR>Technical report IN-062/2002<BR>vi<BR>1.17.1. Technical flight records of the aircraft ............................................................ 34<BR>1.18. Additional information ................................................................................................... 35<BR>1.18.1. Telex to the operators issued by Airbus Industrie ............................................ 35<BR>1.18.2. History of similar cases .................................................................................... 36<BR>1.18.3. Other safety actions carried out by the manufacturer of the aircraft .............. 37<BR>1.19. Useful or effective investigation techniques ................................................................... 37<BR>2. Analysis ................................................................................................................................. 39<BR>2.1. Operation during the Madrid-Tenerife flight .................................................................. 39<BR>2.2. Maintenance actions in Tenerife Norte .......................................................................... 40<BR>2.3. Operation during the flight Tenerife Norte-Madrid-Barajas ............................................ 41<BR>2.4. Actions after the aircraft came to a stop ....................................................................... 45<BR>2.5. Origin of the residual pressure ....................................................................................... 45<BR>2.6. Previous history of residual pressure .............................................................................. 46<BR>2.7. Suitability of the operational procedures ........................................................................ 50<BR>3. Conclusions ............................................................................................................................ 53<BR>3.1. Findings .......................................................................................................................... 53<BR>3.2. Causes ........................................................................................................................... 54<BR>4. Safety recommendations ...................................................................................................... 55<BR>Appendices ................................................................................................................................... 57<BR>Appendix A. Diagram of tracks on runway 33 of Madrid-Barajas Airport ............................... 59<BR>Appendix B. Details of the trouble shooting procedure applied after the incident ................. 63<BR>vii<BR>Technical report IN-062/2002<BR>Abbreviations<BR>00 °C Degrees Celsius<BR>00° 00’ 00’ Degrees, minutes and seconds<BR>AENA «Aeropuertos Españoles y Navegación Aérea», provider of ATC and airport services<BR>AGL Above Ground Level<BR>AMM Aircraft Maintenance Manual<BR>ATC Air Traffic Control<BR>bar Bar, unit of pressure<BR>BDDV Brake Distribution Dual Valve<BR>BITE Built-in test<BR>BSCU Brake & Steering Control Unit<BR>CMM Component Maintenance Manual (i.e. of a master cylinder, valve, etc.)<BR>CMS Central Maintenance System<BR>CVR Cockpit Voice Recorder<BR>DFDR Digital Flight Data Recorder<BR>DH Decision Height<BR>DME Distance Measuring Equipment<BR>E East<BR>ECAM Engine and Crew Alerting Monitoring<BR>FCOM Flight Crew Operating Manual<BR>FOT Flight Operations Telex, communication of Airbus to the operators to inform on operational<BR>issues<BR>ft Feet<BR>g Gravity acceleration<BR>GPWS Ground Proximity Warning System<BR>h: min: sec Hours, minutes, seconds<BR>hPa Hectopascal<BR>IAS Indicated airspeed<BR>IFR Instrument Flight Rules<BR>KCAS Knots of calibrated airspeed<BR>kt Knots<BR>Ibs Pounds<BR>LRU Line Replaceable Unit<BR>m Meter<BR>mb Milibar<BR>METAR Meteorological report<BR>MHz Megahertzs<BR>MLG Main landing gear (there are three legs in the MLG of the A-340: left, centre and right)<BR>N/A Not affected<BR>NLG Nose landing gear<BR>NM Nautical Mile<BR>OIT Operators Information Telex<BR>P/N Part Number<BR>S/N Serial Number<BR>SOP Standard Operating Procedures, prepared by the manufacturer of the aircraft<BR>SSCVR Solid State Cockpit Voice Recorder<BR>TFU Technical Follow-up (communication on in-service difficulties issued by Airbus)<BR>TSM Trouble Shooting Manual<BR>TWR ATC Control Tower<BR>UTC Universal Time Coordinated<BR>ix<BR>Technical report IN-062/2002<BR>Synopsis<BR>On 7 September 2002, at 13:03:27 h, the left and right legs of the main landing gear<BR>of the aircraft Airbus A-340 registration EC-IDF touched down onto runway 33 of<BR>Madrid-Barajas Airport. At that moment, there was a residual pressure of 800 psi on<BR>the alternate hydraulic system of the brakes of the left main landing gear leg. The crew,<BR>that had already detected the presence of that residual pressure at 12:58:02 h when<BR>the WHEEL page of the ECAM was deployed before lowering the landing gear, had<BR>decided to land with the antiskid system disconnected, and had voluntarily moved the<BR>«antiskid & nose wheel steering» switch to the OFF position.<BR>At the beginning of the landing roll, the pilot in command applied reverse, did not press<BR>the brake pedals and used right rudder with the intend of keeping the aircraft aligned<BR>with the runway axis. At a point between 240 m and 900 m beyond the threshold of<BR>runway 33, the four wheels of the left main landing gear leg burst, and the aircraft<BR>deviated initially to the right of the runway axis and then to the left until both crew<BR>members applied full right brake, and the pressure reached 2500 psi on the brakes of<BR>the four right wheels that locked and burst.<BR>Finally, the aircraft came to a stop with the left main landing gear leg at 5m from the<BR>left end of the asphalt area of runway 33, and at 146 m before the axis of the taxiway<BR>J-1, with the fuselage rotated around 10° to the left of the axis of runway 33. The rims<BR>of wheels 1, 2, 4, 5 and 6 suffered heavy damage, as well as the brakes 1, 5 and 6,<BR>due to the drag with the runway surface. There was a fire that affected all the wheels<BR>of the right and left legs of the landing gear, and it was quickly controlled by the fire<BR>fighters of the airport.<BR>Runway 33 remained closed during approximately 6 h and 15 min and there were no<BR>personal damages.<BR>The investigation determined that the cause of the residual pressure in flight was the<BR>left master cylinder P/N C24592020 S/N H2121, which had a length and a dead band<BR>longer than specified.<BR>It is considered that the cause of this incident was the fact that, as a consequence of<BR>the appearance of residual pressure in flight in the left brakes, due to the fact that the<BR>left master cylinder P/N C 24592020, S/N H2121 was defective, and due to the lack of<BR>a procedure to be applied in that case, the crew voluntarily disconnected the antiskid<BR>system when the residual pressure was still present, which produced the burst of the<BR>left tires at touchdown.<BR>The following factors could have prevented the incident:<BR>— The existence in the Operations Manual of instructions to be followed in the case of<BR>residual pressure being observed in flight.<BR>— The knowledge by the affected flight crew of similar cases that had been reported<BR>as complaints during June 2002.<BR>— A more comprehensive analysis of the previous squawks of residual pressure.<BR>— A more detailed training on the brake system during the type rating courses.<BR>Technical report IN-062/2002<BR>x<BR>1. FACTUAL INFORMATION<BR>1.1. History of the flight<BR>1.1.1. Flight Madrid-Tenerife Norte<BR>The aircraft took off from Madrid-Barajas Airport on 7 September 2002, at 06:56 h<BR>UTC1, with 263 people on board (12 crew members and 251 passengers). The destination<BR>was the Airport of Tenerife-Norte. The takeoff weight was 201033 kg and the landing<BR>weight in Tenerife was 184333 kg. The maximum landing weight is 190000 kg.<BR>It was the first flight of the aircraft since 28-7-2002, because it had been repaired after<BR>a bird strike on the nose area that happened on that date.<BR>The flight was normal and, during the approach to runway 12 in Tenerife-Norte, when<BR>the landing gear was lowered at 9:19:24 h, the copilot noticed that in the wheel page<BR>of the ECAM there were indications of residual pressure in the brakes of the left MLG.<BR>The 24 bars that represent the brakes of the 4 wheels of that landing gear were lit in<BR>amber colour.<BR>The crew considered that this indication, which is not associated to any caution message,<BR>could be spurious, and for that reason they decided to land without additional<BR>measures.<BR>The aircraft continued the approach with the antiskid system connected and with the<BR>autobrake systems disconnected. After switching off the autopilot, the copilot was<BR>the PF during the approach and landing in manual mode with the autothrust connected.<BR>After touching down, according to his statement, the copilot noted that the aircraft started<BR>deviating to the left of the runway, and therefore applied progressively right rudder<BR>until reaching full deflexion. Then he applied brakes, initially right toe brake and then<BR>both brakes, always steeping more the right pedal, until the aircraft, which initially had<BR>approached at around 8 m from the left side of the runway 12, deviated towards the<BR>right and finally came to a stop with its centre of gravity separated around 5 m to the<BR>right of the runway axis.<BR>The DFDR data show that at the moment of the landing there was a pressure of 900<BR>psi in the left alternate brake system. After the left and right legs touched the ground<BR>at 9:21:43 h and the spoilers started to deploy, the brake pedals were not pressed, and<BR>therefore the alternate system remained active and the 900 psi of pressure were trans-<BR>1<BR>Technical report IN-062/2002<BR>* All the times used in this report are UTC, except where specifically noted. It is necessary to add two hours to have<BR>the local time in Madrid-Barajas Airport, and one hour to have the local time in Tenerife-Norte Airport.<BR>mitted to the wheels. The copilot used more and more right rudder to counteract the<BR>increasing tendency to veer to the left as the airspeed was decaying. Within 9:21:50 h<BR>and 9:22:03 there were small movements of the right brake pedal, of around 8° (the<BR>following angle values correspond to the pedal potentiometer; the maximum deflexion<BR>of the pedal corresponds to a pedal potentiometer position of 68.80°; the maximum<BR>physical pedal deflexion is 14°11’) that were not enough to send pressure to the normal<BR>brake system until 9:22:03 h, at which moment both pedals were pressed (52° the<BR>right pedal and 26° the left pedal), the normal system was pressurized and the residual<BR>pressure of the alternate system was released. From that moment on, the aircraft behaviour<BR>regarding braking was normal.<BR>The tower said to the crew at 9:27:10 h that they could vacate the runway at their discretion<BR>and the crew of EC-IDF answered that they had a brake problem and they would<BR>call back when ready to leave the runway.<BR>The tower advised another traffic that was in short final to be ready to go around<BR>because the runway was occupied.<BR>The crew of EC-IDF switched off and then on the BSCU. The residual pressure had<BR>disappeared. At 9:27:43 h, they told the tower controller that they were going to<BR>leave the runway «through the first on the left» and started a taxi by their own<BR>means until they confirmed «runway vacated» at 9:29:25 h and asked for the possibility<BR>to stay at that point of the taxiway for a few minutes. The tower requested<BR>them to move a little more forward because they still protruded a little bit over the<BR>runway.<BR>The aircraft moved as requested and at 9:29:52 h they said that they were proceeding<BR>to the parking apron. The tower asked whether they needed towing or were able to<BR>move by their own means, and also whether they needed further help.<BR>The crew answered that they would taxi by their own means. At those moments, they<BR>were noting that the temperature of the four brakes of the left MLG was increasing a<BR>lot, and called their ground operations department to advise that maybe a maintenance<BR>action was going to be needed. Operations asked whether fire fighting services were<BR>going to be needed and the pilot in command answered in the positive and requested<BR>that nobody approached the aircraft.<BR>At 9:33:35 h, the flight that had landed after EC-IDF called tower to advise that they<BR>were seeing smoke coming out from the «left rear wheel» of that aircraft.<BR>The crew of EC-IDF acknowledged the information and thanked for it. The temperature<BR>of the wheels of the left MLG had continued increasing until an ECAM caution was<BR>triggered. The aircraft contacted ground movement frequency at 9:35:36 h and the controller<BR>asked whether they needed that the fire fighters applied water or preferred the<BR>Technical report IN-062/2002<BR>2<BR>wheels to be cooled alone. The crew answered they were going to check with the maintenance<BR>personnel and finally rejected the offer to apply water.<BR>1.1.2. Stop in Tenerife Norte<BR>CWhen the aircraft reached the parking, chocks were put in the wheels and the brakes<BR>were cooled using two fans provided by the line maintenance of the operator and another<BR>provided by the fire fighters that were around the aircraft. The passengers disembarked<BR>the aircraft in a normal way.<BR>According to his statement, the pilot in command informed the ground maintenance<BR>personnel about the incidence during the landing and it was commented that the problem<BR>would be consulted with the operator’s main base in Madrid.<BR>According to their statement, the maintenance personnel entered the cockpit and saw<BR>the high brake temperature caution and observed in the post-flight report that there<BR>had been a caution of «Brakes residual braking». They tried to test the BSCU 1 and 2<BR>but they were unable to do that.<BR>The information gathered shows that while the maintenance personnel were trying to<BR>locate technical advice in the Madrid base, the passenger boarding of next flight Tenerife-<BR>Madrid started, with the same flight crew that had flown the previous leg.<BR>Some information was interchanged with the pilot in command, who understood that<BR>the maintenance personnel had no inconvenience for the starting of the flight back to<BR>Madrid. However, these personnel were still considering the possibility of lifting the left<BR>MLG to check the free movement of the wheels, although in the end this action was<BR>not carried out because during the previous taxi to the apron the wheels seemed to<BR>have behaved correctly.<BR>Once the boarding ended, a person from maintenance Madrid called the line maintenance<BR>Tenerife and was informed about the situation. Since in the ECAM screen there<BR>was no caution, and the brake temperature had fallen within normal limits, this conversation<BR>did not produce further maintenance actions and therefore the doors were<BR>closed and the aircraft started the taxi for takeoff.<BR>The maintenance personnel advised the pilot in command to watch the temperature<BR>during the taxi just in case a new cooling was needed. The aircraft taxied normally, and<BR>the pilot in command informed that after the takeoff he would leave the landing gear<BR>down for some minutes to further cool it.<BR>In the aircraft logbook the crew did not write any squawk after the landing in Tenerife.<BR>The maintenance personnel wrote that the normal «transit» line check was comple-<BR>3<BR>Technical report IN-062/2002<BR>ted, but they did not report any of the actions carried out on the brake system. Neither<BR>in that flight nor in next flight (Tenerife-Madrid where the incident happened) was the<BR>aircraft acceptance form signed by the pilot in command.<BR>1.1.3. Flight Tenerife Norte-Madrid<BR>The aircraft, with the flight identifier IB-0959, took off around 10:55 h from Tenerife,<BR>after a taxi of 5 min since the moment of chocks off during which the general behaviour<BR>of the aircraft was checked and it was confirmed that no new cautions appeared.<BR>The takeoff was normal, with a weight of 173404 kg, compared with the maximum<BR>takeoff weight of 275000 kg. There were 247 passengers and 12 crew members on<BR>board.<BR>The brake temperatures were still slightly high, and therefore the crew left the landing<BR>gear down for several minutes after lift-off.<BR>The flight progressed normally. The crew did not show excessive concern with respect<BR>to the reappearance of the failure in Madrid.<BR>At 12:58:02 h, with the landing gear still up, the copilot called the WHEEL page of the<BR>ECAM and they saw again the there was residual pressure in the brakes of the left MLG,<BR>because the bars that represented the brakes appeared again in amber colour. The crew<BR>disconnected and then connected the BSCU but the amber bars did not disappear.<BR>At 12:58:38 h landing gear down was selected, the system started its normal self-checks<BR>and the residual pressure disappeared momentarily but almost immediately appeared<BR>again. The crew again disconnected during 24 s and then connected the BSCU,<BR>although this action, not permitted by the operational procedures when the landing<BR>gear is extended, did not succeed in eliminating the residual pressure indication.<BR>Since the moment they noticed there was residual pressure in the left leg, both pilots<BR>were commenting the possible actions to be taken. It was discussed the possibility of<BR>discontinuing the approach, and it was commented that the only solution would be to<BR>disconnect the antiskid because in that case the system was not going to brake by itself,<BR>and, therefore, to lock the wheels.<BR>Finally, the copilot disconnected the antiskid system and nose wheel steering switch<BR>after asking the pilot in command for conformity.<BR>The aircraft continued its approach to runway 33 of Madrid-Barajas Airport with the<BR>pilot in command acting as PF. The aircraft configuration was flaps down and landing<BR>Technical report IN-062/2002<BR>4<BR>gear down, without autopilot but with autothrust connected, and with the antiskid and<BR>the autobrake off. The spoilers had not been armed during the approach.<BR>The pilot in command, taking into account the low weight and the length of the runway<BR>in Barajas, had decided to touchdown as soon as possible onto the runway and to<BR>apply thrust reverse, without touching the brakes as long as it was not indispensable.<BR>There was no communication to the passengers or cabin crew, and the ATC was not<BR>informed that there could be some problem with the aircraft.<BR>The approach continued and the pilot in command recalled after the incident that the<BR>aircraft touched the ground over the numbers of runway 33. The left and right MLG<BR>touched down around 13:03:27 h and the reversers were selected three seconds afterwards.<BR>The central MLG and the NLG touched down at around 13:03:32 h. At the<BR>moment the main legs touched down, the spoilers did not deploy, because they were<BR>not armed.<BR>When the reversers were deployed, the spoilers deployed in accordance with the<BR>system design, which always deploys them even when they were not armed during<BR>the approach.<BR>At the first moment they touched down the wheels of the left leg were braked with<BR>around 800 psi of residual pressure. The pilot in command, without pressing the brake<BR>pedals, applied progressively more and more right rudder to try to keep the aircraft aligned<BR>with the runway axis.<BR>At 13:03:45 h the right brake pedal was pressed up to the limit, which made the pressure<BR>to increase up to around 2500 PSI and the wheels of the right MLG burst in that<BR>area.<BR>Finally the aircraft came to a stop at 13:04:01 h in such a manner that the left leg<BR>remained at around 146 m before the axis of the taxiway J-1 (the first exit after the<BR>intersection of runways 33 and 36L) and at around 5 m from the end of the paved runway<BR>shoulder, that is, it has crossed the line of the lateral runway edge lights. The longitudinal<BR>axis of the aircraft had turned around 10 degrees to the left with respect to<BR>the axis of runway 33 and, therefore, the nose MLG leg also remained at approximately<BR>5 m away from the lateral end of the paved runway shoulder.<BR>1.1.4. Actions taken after landing and evacuation of the passengers<BR>After the aircraft came to a stop, the crew informed the tower that they had a problem<BR>with the brakes and that they were going to remain on the runway. The ATC commanded<BR>the next aircraft that was approaching to runway 33 to go around and called<BR>the fire fighters.<BR>5<BR>Technical report IN-062/2002<BR>At around 13:04:32 h, that is, approximately 30 s after the aircraft came to a stop, the<BR>aircraft that was going around informed by radio that the EC-IDF had fire on the wheels.<BR>The air traffic controller answered that with so much smoke she could not really see<BR>what had happened. Then she commanded another aircraft to go around.<BR>When they heard the information about fire on their wheels, the crew of EC-IDF decided<BR>to shut down the engines. For several minutes, they were evaluating the possibility<BR>of ordering an emergency evacuation of the airplane. After 3 min and 8 s since the aircraft<BR>stopped, the flight crew addressed the passengers to advise them to remain seated<BR>without using the mobile telephones.<BR>At 13:06:22 h the crew called by radio their Operations Department to request assistance<BR>to transport the passengers and to tow the aircraft. They called then tower to ask<BR>for confirmation that only smoke was present in the wheels and on their side informed<BR>the air traffic controller that the fire fighters were already around the aircraft. The tower<BR>answered saying that it was confirmed that the fire was extinguished and asked for the<BR>possibility of the aircraft to taxi to leave the runway.<BR>When she received a negative answer from the flight crew, that suspected that they<BR>had all the wheels burst, the air traffic controller commanded other aircraft to go<BR>around while in the airport several services started to coordinate and communications<BR>were held with approach control services after the local alarm was activated. The surface<BR>of runway 36R was inspected and was open for arrival traffic around 13:16 h, while<BR>runway 36L was still active for takeoffs.<BR>In the meanwhile, inside the aircraft, the crew said to the passengers that there had<BR>been a problem with the brakes and that coaches would arrive soon to take them from<BR>the aircraft to the terminal. This address took place after a request of the pilot in command<BR>4 min and 8 s (13:08:09 h) after the aircraft stopped.<BR>Technical report IN-062/2002<BR>6<BR>At 13:24 h the passengers started coming out the aircraft using door 1R and a stairway<BR>provided by the ground handling personnel. When all the passengers had left the aircraft,<BR>the crew also evacuated it. The passengers were taken to the terminal by shuttle<BR>coaches.<BR>The maintenance personnel of the operator replaced all the wheels of the left and right<BR>MLG and around 18:25 h the aircraft was towed towards the maintenance hangars.<BR>The area was cleaned and runway 33 and its lighting system were inspected. At 19:21<BR>h runway 33 was again open for arrival traffic.<BR>1.2. Injuries to persons<BR>Injuries Fatal Serious Minor/none<BR>Crew 12<BR>Passengers 251<BR>Others<BR>1.3. Damage to aircraft<BR>The eight wheels of the left and right MLG burst during the landing roll, and the wheel<BR>rims dragged over the runway surface. The lower part of the four left brake assemblies<BR>was totally disintegrated as a consequence of the contact with the ground. The<BR>eight wheels and their brake assemblies were replaced.<BR>After the incident, following a troubleshooting procedure prepared by Airbus (see 1.16)<BR>and before any further flight, the left brake master cylinder P/N C24592020, S/N H2121,<BR>was also replaced.<BR>The left leg assembly of the MLG had eventually to be completely replaced, because of<BR>the loads suffered during the landing roll once the wheels had burst. There was fire on<BR>all the wheels of the left and right MLG, but no other part of the aircraft was affected<BR>by that fire.<BR>1.4. Other damage<BR>After a visual inspection, it was determined that there was no appreciable damage to<BR>the paved surface of runway 33 of Barajas airport. Therefore, there was no other<BR>damage in addition to those to the aircraft.<BR>7<BR>Technical report IN-062/2002<BR>1.5. Personnel information<BR>1.5.1. Pilot in command<BR>Age: 59 years old<BR>Nationality: Spanish<BR>Title: Airline Transport Pilot<BR>Licence: Valid since 21-1-2002 until 21-1-2007<BR>Type rating: Pilot in command A-340. He had also flown DC-9, B-<BR>727 and A-300<BR>Total flight time: 10439 h<BR>Hours in the type A-340: 3250 h<BR>Hours in the last 90 day: 175 h<BR>Latest simulator check: 8-4-2002<BR>He attended the A-340 pilot in command type rating course in Iberia within 12-5-1997<BR>and 13-7-1997, with a flight instructor that got his rating in Airbus/Miami. Afterwards,<BR>he attended the following two-day recurrent training courses also in Iberia:<BR>January 1998; July 1998; March 1999; November 1999; June 2000; November<BR>2000; January 2001; July 2001.<BR>On 8 April 2002 he renewed the type rating after some sick leave.<BR>The pilot in command had flown last time on 29 August before initiating a new activity<BR>period on 7 September at approximately 5:50 h.<BR>1.5.2. Copilot<BR>Age: 33 years old<BR>Nationality: Spanish<BR>Title: Airline Transport Pilot<BR>Licence: Valid until 29-10-2006<BR>Type rating: Copilot A-340. He had also flown MD-87<BR>Total flight time: 2310 h<BR>Hours in the type A-340: 1420 h<BR>Technical report IN-062/2002<BR>8<BR>Hours last 90 days: 210 h<BR>Latest simulator check: 27-10-2001<BR>He attended the A-340 type rating course in Iberia within 23-6-2000 and 17-8-2000,<BR>with a flight instructor that got his rating in Airbus/Miami. Afterwards, he attended the<BR>following two-day recurrent training courses also in Iberia:<BR>July 2001; October 2001; May 2002.<BR>The copilot had flown last time on 6 September, and had had 16 h and 30 min of rest<BR>before initiating a new activity period on 7 September approximately at 5:50 h.<BR>1.5.3. Type rating training<BR>The Training Manual of the operator was reviewed and it was found that the initial<BR>type rating course included 6 h of ground instruction devoted specifically to electrical,<BR>hydraulic, landing gear and APU systems. Later on, the second session in flight simulator,<BR>which had an estimated time of completion of four hours, was devoted to<BR>ECAM, actions after failures, and hydraulic and electrical systems with generated failures<BR>and the corresponding ECAM actions. The operator stated that they used as a<BR>base the Airbus recommended training syllabus and procedures as included in the Airbus<BR>«A340 Flight Crew Training Manual», from which they provided the investigation<BR>with the relevant pages of the «Standard Course». Additionally, they stated that their<BR>refreshment courses covered all the systems of the aircraft every two years, i.e. one<BR>year below the JAA requirement of three years to complete the review of all the<BR>systems.<BR>After the incident, the manufacturer reviewed their syllabus for A-340 type rating in the<BR>part relative to brakes and they concluded that their recommended syllabus was adequate<BR>and no change was needed. No information was gathered regarding the details<BR>of the residual braking training recommended or provided.<BR>1.6. Aircraft information<BR>1.6.1. Airframe<BR>Make: Airbus<BR>Model: A-340-313<BR>Serial number: MSN 474<BR>9<BR>Technical report IN-062/2002<BR>Registration: EC-IDF<BR>Year of manufacture: 2002<BR>M.T.O.W.: 275000 kg<BR>Operator: Iberia L.A.E.<BR>Total flight time: 960 FH<BR>Total flight cycles: 133 FC<BR>1.6.2. Description of the brake system of the A-340-313<BR>According to the description of the Operations Manual prepared by the operator of the<BR>aircraft, the A-340 has brakes in the wheels of the right and left MLG (the central leg<BR>of the MLG does not have brakes) that may be applied by any of the two independent<BR>brake systems (normal system, or green system, and alternate system, or blue system).<BR>There are also autobrake and antiskid.<BR>The brake commands may come from the pilot, when the brake pedals are pressed, or<BR>from the autobrake, with a deceleration rate previously selected by the crew. When in<BR>normal mode, all those commands are controlled by the Brake System Control Unit<BR>(BSCU) that has two channels. The alternate (blue) system is hydromechanical.<BR>This BSCU also checks the residual pressure and the temperature of the brakes and provides<BR>information on the speed of the wheels to other systems of the aircraft.<BR>In flight, only the alternate system is pressurized and available. During landing, the brakes<BR>revert to the normal system at the moment the brake pedals are pressed or at the<BR>moment of touchdown if the autobrake system is armed.<BR>When the normal system pressurizes and is active, the feed of pressure to the alternate<BR>system is automatically cancelled. The brakes also momentarily revert to the normal<BR>system in flight when the landing gear is lowered, while several auto tests are being<BR>performed in the brake system.<BR>1.6.2.1. Antiskid system<BR>The antiskid system provides a maximum braking efficiency maintaining the speed of<BR>the wheels at the limit of slipping. The antiskid function is automatically disconnected<BR>on ground when the speed is below 10 kt. There is a switch (A/SKID & N/W<BR>STRG) in the cockpit with to positions (ON/OFF) that allows the manual connection<BR>and disconnection of the antiskid and the nose wheel steering functions at the<BR>same time.<BR>Technical report IN-062/2002<BR>10<BR>The antiskid system never increases the pressure by itself, but simply releases or maintains<BR>the pressure applied by other parts of the system (the pedals or the autobrake).<BR>1.6.2.2. Autobrake system<BR>This system reduces the delay in the braking action in the event of an acceleration-stop<BR>to improve the performances and establishes and maintains a deceleration rate during<BR>landing to improve the comfort and reduce the workload of the flight crew.<BR>The system may be armed before the landing pushing the switches LO, MED or MAX<BR>(braking rate low, medium or maximum) under certain conditions, including that the<BR>antiskid system must be electrically energized.<BR>During the landing roll the autobrake action starts with the command to extend the<BR>spoilers.<BR>The normal procedures of the operator (Operations Manual A340, 2.01.63, 4-12-2000)<BR>indicate that in final the autobrake may be selected at LO or ME («if required») and<BR>then add: «In the event of crosswind, contaminated or short runway, or under low visibility<BR>conditions, select LO or MED. In a dry runway of normal length, normally the use<BR>of autobrake is not necessary».<BR>However, the procedures recommended by the manufacturer of the aircraft indicate:<BR>«Use of the autobrake is recommended.<BR>Use of MAX mode is not recommended at landing.<BR>On short or contaminated runways, use MED mode.<BR>On long and dry runways, LO mode is recommended.<BR>Note: If, on very long runways, the pilot anticipates that braking will not be needed,<BR>use of the autobrake is unnecessary.<BR>Press the appropriate pushbutton, according to runway length and condition, and<BR>check that the related ON light comes on.«<BR>1.6.2.3. Brake modes<BR>There are four modes of operation of the brakes:<BR>A) Normal braking: when there is hydraulic pressure of the first system, called green<BR>hydraulic pressure and the switch A/SKID & N/W STRG is in ON, among other conditions.<BR>The control is electrical through the BSCU, and the braking command is<BR>provided with the pedals or automatically by the autobrake (on ground) or when<BR>11<BR>Technical report IN-062/2002<BR>the landing gear lever is moved to «UP» (in flight). There is no indication to the<BR>crew of the hydraulic pressure applied to the brakes.<BR>B) Alternate braking with antiskid: when the normal or green hydraulic pressure is not<BR>enough, and the switch A/SKID & N/W STRG is in the ON position, there is an automatic<BR>selection of the blue or second hydraulic system, and the alternate braking<BR>system is available. In this case, the control is achieved through the pedals through<BR>an auxiliary low pressure circuit that actions the DUAL valve. The BSCU continues<BR>controlling the antiskid system. The pressure sent to the left and right brakes, and<BR>the pressure of the accumulator, appear in a triple indicator located in the centre<BR>of the instrument panel (see Figure 1).<BR>It is important to note that the pressure transducer to the triple indicator and to<BR>the ECAM indication is the same. For this reason, spurious indication of residual<BR>pressure may occur in the ECAM and in the triple indicator at the same time, and<BR>those transducers were mentioned in the TFU (see 1.6.3) as a common cause of<BR>the false residual pressure indication.<BR>C) Alternate braking without antiskid: If the switch A/SKID & N/W STRG is manually<BR>moved to the OFF position, or there is a failure in the electrical supply or failure<BR>of the BSCU, or when there is a low hydraulic pressure in both the green and<BR>blue systems, the antiskid system is disconnected. The control is achieved through<BR>the pedals, that actuate the DUAL valve, while the servo valves of the alternate<BR>system are fully open and all the pressure commanded by the pedals reach<BR>Figure 1. View of the triple indicator of pressure. The landing gear is down, but the antiskid<BR>switch is in OFF. Therefore, the vertical bars that represent the brakes of every wheel do not<BR>appear in the WHEEL page of the ECAM screen<BR>Technical report IN-062/2002<BR>12<BR>directly the brakes, and therefore the pilot has to regulate the pressure with the<BR>pedals with reference to the triple indicator to avoid the lock and burst of the<BR>wheels.<BR>D) Parking brake: In this mode the brake receives the hydraulic pressure of the blue<BR>system or of the accumulator through the DUAL valve. This brake may be used in<BR>emergency.<BR>1.6.2.4. Indications, warnings and cautions<BR>In addition to the triple indicator mentioned above, the WHEEL page of the ECAM<BR>(«Engine indication and alert monitoring») presents a schematic indication of the eight<BR>wheels of the MLG that have brakes (four on the left leg and four on the right leg)<BR>together with additional information on the brake system, including the status of the<BR>antiskid system, of the autobrake system (AUTO BRK), rate of autobrake selected (MED),<BR>and brake temperature (F in the attached Figure 2) of every wheel (numbered as shown<BR>in item D in the attached figure).<BR>Figure 2. Wheel page of the ECAM<BR>13<BR>Technical report IN-062/2002<BR>On the other hand, in both sides of each wheel three vertical bars appear (item E in the<BR>Figure 2) that represent the brakes of that side of the wheel. They appear in green<BR>colour in flight, when the landing gear is down and the antiskid is operative, and on<BR>ground when the brakes are released and the antiskid is active. They appear in amber<BR>colour in the event that there is residual pressure or if there is a failure in the release<BR>of the brakes.<BR>The indication R («release») always appears in white colour.<BR>There is residual pressure whenever, with the brakes released, some pressure is trapped<BR>anywhere in the normal or alternate systems. On ground, when the pressure of at least<BR>one wheel is above 15 bar with the pedals released, there is a «Master Caution» with<BR>audible sound and visual indications in the page WHEEL of the ECAM. This caution is<BR>inhibited in the ground when the speed is higher than 80 kt and during takeoff, climb,<BR>cruise, descent and landing until the speed is below 80 kt.<BR>The page WHEEL is automatically shown in the ECAM every time «landing gear down»<BR>is selected, even when there is no caution or warning in the system.<BR>1.6.2.5. Schematics of the alternate brake system<BR>A brief and schematic description of the physical layout of the brake system of the A-<BR>340 is presented here below, together with its situation when the alternate system is<BR>working. For that purpose, the attached Figure 3, copied from a familiarization training<BR>course of the manufacturer.<BR>As it can be seen in the figure, the automatic selector allows the pressure of the alternate<BR>or «blue» system is feeding the brake circuit. The brake distribution dual valve<BR>(BDDV) or «dual valve» is a very important component of the system, and each of its<BR>sides is activated by an auxiliary low pressure circuit that comes from the pedal of that<BR>side. When the pedal is pressed, that low pressure activates the corresponding side of<BR>the BDDV (as represented in the figure), in such a way that the blue pressure reaches the<BR>«alternate servo valve». This servo valve opens or closes as controlled by the BSCU that<BR>in turn receives information from the antiskid when it is active, as it happens in the condition<BR>represented in the figure. In such a case, the pressure is regulated to keep an optimum<BR>rate of braking with a certain amount of slip of the wheels determined by the<BR>design of the system and the wheel do not lock even when the pedals are fully pressed.<BR>However, if the switch A/SKID & N/W STRG that can be seen in the figure is moved to<BR>the OFF position, the BSCU is disconnected and the servo valve is fully open, and therefore<BR>any hydraulic pressure of the blue system called upon by the BDDV is transmitted all<BR>along to the brakes. Under those conditions, the pilot must carefully watch the triple<BR>indicator (also represented in the figure) to keep the pressure on each side or leg of the<BR>MLG at 1000 psi as a maximum, because otherwise there is a risk to lock the wheels and<BR>almost certainly burst them.<BR>Technical report IN-062/2002<BR>14<BR>Figure 3. Schematics of the brake system. The alternate system is operating with the antiskid<BR>system ON in the represented condition<BR>When the alternate brake system is active, each pedal applies pressure to the auxiliary<BR>low pressure system through a master cylinder that can be seen in figures 1.6.2.5.2 and,<BR>in greater detail, 1.6.2.5.3. When there is no force F applied, the chambers C1 and C2<BR>are communicated and full of hydraulic fluid because the valve is kept outside its seating<BR>by the spring R2. When the pedal is pressed (force F) the sliding assembly is compressed<BR>downwards against spring R2 and there is initially a dead travel. The hydraulic<BR>fluid goes from chamber C1 to chamber C2 and comes out through port B. If the pedal<BR>deflexion continues, when the dead travel ends, and the preformed packing moves with<BR>the sliding assembly up to it is pressed against the valve, in such a way that the flow<BR>between chambers C1 and C2 is cut, and pressure in chamber C1 starts raising. The sliding<BR>assembly moves the valve and presses springs R1 y R2 and produces the reduction<BR>of the volume of chamber C1 and the fluid flows out through port A towards the dual<BR>valve (BDDV). The pressure in chamber C1 is proportional to the resistance opposed by<BR>the hydraulic fluid in the external system connected to port A.<BR>If the brake system is in normal mode (with green hydraulic pressure), the movement<BR>of the pedals is electronically sent to the BSCU that processes the intention of the pilot<BR>and the information of the antiskid system to command directly the normal servo valve<BR>and to apply the corresponding pressure to the wheels. The dual valve does not work<BR>in that condition.<BR>15<BR>Technical report IN-062/2002<BR>Figure 4. Drawing of the master cylinder. When the pedal is pressed, a force F is applied in the<BR>upper part of the cylinder<BR>Technical report IN-062/2002<BR>16<BR>Figure 5. Detailed cutaway of the master cylinder<BR>17<BR>Technical report IN-062/2002<BR>According to the Component Maintenance Manual (CMM) «Master Cylinder C24592020»,<BR>dated 31 July 1992, the total length of the cylinder must be between 170.050 mm and<BR>170.100 mm, and the dead band must be between 0.4 mm and 0.5 mm (there was a<BR>typo in the CMM, page 703, in which it is mentioned «dead travel 0,4 to 05»).<BR>1.6.3. Abnormal and emergency procedures related to the<BR>brake system<BR>1.6.3.1. Abnormal procedures<BR>The Operations Manual prepared by the operator in Spanish language, Paragraph 3-<BR>02.32, dated 20-3-2001, mentions two abnormal procedures related to the circumstances<BR>of the event:<BR>«BRAKES A/SKID FAULT» AND «BRAKES A/SKID NWS OFF»: (English translation) The first<BR>warning appears in the event of antiskid failure and the second when the switch A/SKID<BR>& N/W STRG is in OFF. In both cases, the maximum brake pressure must be 1000 PSI, and<BR>the brake pressure must be watched in the triple indicator. The effect of brake application<BR>is much higher than in normal mode and therefore the pedals must be pressed smoothly<BR>without exceeding the mentioned pressure. The landing distance increases by 1.4.<BR>«BRAKES RESIDUAL BRAKING» (dated 30-4-2002): (English translation) If the warning<BR>appears on ground, immediately after engine start or during taxi, make a reset of the<BR>BSCU selecting the switch A/SKID & N/W STRG to OFF. If the warning does not disappear<BR>a maintenance action is required. NOTE: to make the reset of the BSCU it is needed<BR>that the aircraft is still and the parking brake applied. The indication «ON BRAKE 1<BR>(2, 3, 4, 5, 6, 7, 8») appears for the information of the crew when there is brakes residual<BR>pressure affecting one or two wheels.<BR>In this latter case that brakes residual pressure appears in any of the wheels (amber bar<BR>on those wheels) there is no instructions about what the crew must do. There is no clear<BR>indication in the abnormal procedure whether the warning appears in flight, on<BR>ground or in both cases (see 1.6.4.4. above with the description of this indication copied<BR>from the Operations Manual, Chapter «Systems»).<BR>For the understanding of the circumstances of the incident described in this report, it is<BR>very important to distinguish between the CAUTION of «brakes residual pressure» and<BR>the INDICATION of «residual pressure in wheel(s) number X, Y...».<BR>— The caution consists of an audible gong, MASTER CAUTION light, and the text<BR>«RESIDUAL BRAKING», and may only appear on ground. In flight the caution is inhibited,<BR>even though there is actual residual pressure. When it appears on ground, the<BR>Operations Manual of the operator requests that a reset of the BSCU be made and,<BR>if the caution continues, to call Maintenance.<BR>Technical report IN-062/2002<BR>18<BR>— The INDICATION (vertical bars in amber colour in one or more wheels) may appear<BR>on ground or in flight when the page WHEEL of the ECAM is displayed, which<BR>always happens automatically when landing gear is selected down. When this indication<BR>appears, the Operations Manual does not provide any procedure to be followed.<BR>The Flight Crew Operating Manual (FCOM) prepared by the manufacturer of the aircraft<BR>differs from that prepared by the operator about the actions to be taken in the event<BR>a «RESIDUAL BRAKING» caution is displayed (always on the ground), because there is<BR>no mention to make a reset of the BSCU, but simply to call Maintenance.<BR>However, the SOP of Airbus does require making a reset of the BSCU in Chapter «Supplementary<BR>Techniques» (3.04.32 P1) where they say: «In case of braking/steering difficulty,<BR>the crew may perform a BSCU reset to recover correct functioning of the system.<BR>In particular, this applies to the following ECAM Warnings: ... Brakes residual warning».<BR>Also the «Technical Follow-up» issued to cover the appearance of residual pressure in<BR>flight and the «Flight Operations Telex» on the same subject (see paragraph 1.6.3) mentioned<BR>the possibility of making a reset of the BSCU.<BR>The SOP of the manufacturer do not allow making a reset of the BSCU in flight with<BR>the landing gear down.<BR>The FCOM de Airbus did not provide, in the date of the incident, instructions about<BR>what to do if INDICATION (amber bars) of residual pressure was noticed in some wheel<BR>during flight.<BR>1.6.3.2. Emergency procedures<BR>The only emergency procedure related to the brake system included in the Operations<BR>Manual of the operator (3.01.32, 1-10-2000) is the following:<BR>«PÉRDIDA DE FRENADA»: (English translation) if brakes are not available, maximum<BR>thrust reverse, release the brake pedals, disconnect the switch A/SKID & N/W STRG,<BR>carefully press the brake pedals, limit the brake pressure to 1000 PSI, check the<BR>BRAKES PRESS indicator, and maintain directional control with differential braking<BR>as the nose wheel steering is not available. If still brakes are not available, the parking<BR>brake must be used making short and continuous applications of the parking<BR>brake to stop the aircraft. At the beginning of each parking brake application some<BR>asymmetric braking could appear. When ever possible, the application of the parking<BR>brake must be delayed until the speed has decreased, to reduce the risk of tire<BR>burst and difficulties in directional control.<BR>19<BR>Technical report IN-062/2002<BR>1.6.3.3. Checklist in final<BR>The Operations Manual prepared by the operator, Chapter 2.01.63, 15-10-2001, says that<BR>«(English translation) The checklist of FINAL is read by the PNF, at request of the CM-1,<BR>and is answered by the CM-1 and the CM-2 as applicable. Its completion guarantees<BR>that the aircraft is safe for landing. The checklist of FINAL appears in the E/W D of the<BR>ECAM below 1500 ft with the landing gear extended.»<BR>«A/THR CHECKED SPEED OR OFF<BR>LDG SIGNS ON<BR>LDG GEAR DN<BR>FLAPS LDG<BR>SPLRS ARMED<BR>Checklist of FINAL completed.»<BR>1.6.4. Previous maintenance on the aircraft<BR>The aircraft suffered a bird impact in the nose area on 28-7-2002, when it was approximately<BR>at 7000 ft of altitude, and as a consequence repair maintenance was carried<BR>out in which a technical team of the manufacturer provided on site support, and during<BR>which the brake pedals were disassembled and then assembled again as a whole<BR>assembly, in other words, the subcomponents of the pedal assemblies were not dismounted.<BR>After the repair, the team of the manufacturer conducted a complete operational<BR>test of the alternate brake system, according to AMM Task 32-43-00-710-801.<BR>The results were OK.<BR>At that time, a scheduled inspection A-2 was carried out when the aircraft had 957 h<BR>of flight.<BR>The day of the incident the aircraft made its first flight after those maintenance tasks.<BR>1.6.5. Previous incidences in the brake system of aircraft EC-IDF<BR>The following abnormalities related to the event were reported in June 2002:<BR>Date Abnormality Corrective action taken<BR>07-06-02 When the LG is lowered residual pressure<BR>appears in left wheels 1, 2, 5 and 6 with<BR>subsequent heating.<BR>08-06-02 In descent with clean configuration the brakes<BR>residual braking lights on brake 1, 2, 5<BR>and 6, at parking 500 °C+ of temperature<BR>reached.<BR>Carried out System Test BSCU channels 1 and<BR>2 Test OK. Carried out System Test BSCU<BR>«Norm BRK» in channels 1 and 2 Test OK.<BR>Test of BSCU channel 1 and 2 results correct.<BR>Technical report IN-062/2002<BR>20<BR>According to the information gathered, those abnormalities were not reported to the<BR>manufacturer. However, similar squawks were reported to Airbus in year 2001 due to<BR>the residual pressure that appeared in aircraft EC-GUP.<BR>Late in the investigation process, the operator stated that AMM Task 32-43-00-710-801<BR>«Operational test alternate brake system» was carried out on 11 June 2002 (the day of<BR>the last squawk). They said that, although the task was not specifically recorded on the<BR>logbook, the technician recorded other actions like checking the free rotation of the<BR>wheels that are a part of the task. This is the last action to be carried out after the application<BR>of TSM task 32-40-00-810-927 (see below). Regarding this task, they also stated<BR>that the «fault confirmation» (look at the triple indicator to see if there is pressure) was<BR>also carried out on 11 June 2002 (see table above).<BR>The manufacturer was indeed aware of other indications of residual pressure, and they<BR>had issued the «Technical Follow-up» (TFU) 32.42.21.002 «Brakes residual braking<BR>ECAM warning» in September 2000 in which it was mentioned that the warning used<BR>to be due to a spurious indication, caused by the pressure transducers or by the monitoring<BR>of the BSCU, although it was also stated that the residual pressure could also be<BR>real. The TFU mentioned the possibility of resetting the BSCU using the switch of the<BR>antiskid. The TFU also called for two troubleshooting procedures, which would detect<BR>whether the pressure indication was real or spurious. Both tasks (32-40-00-810-839 and<BR>21<BR>Technical report IN-062/2002<BR>Date Abnormality Corrective action taken<BR>09-06-02 In the landing the message residual Braking<BR>appears in wheels of left leg (N° 1-2-5-6), it<BR>disappears after a reset in the parking.<BR>10-06-02 In approach residual pressure in left leg<BR>brakes. Solved after several resets of Nose<BR>Wheel Stering switch (there was indication<BR>of pressure in the brake indicator) and pressing<BR>the brakes at the same time. See previous<BR>reports.<BR>11-06-02 At landing appears in the ECAM «Residual<BR>Brakes» in the left leg.<BR>The servovalve connectors are cleaned and<BR>the pressure transducer of wheels associated<BR>(9GG1, 10GG1, 11GG1, 12GG1 and 5-<BR>6-7-8GG1). It is inspected the status and<BR>condition of dual valve (5403GG), Master<BR>Cylinder (5422GG) and filter LP-B RSVR<BR>(5011JM2) and no abnormalities found.<BR>System Test and Normal BRK Test of both<BR>BSCU OK.<BR>Test of BSCU and reset of the brake system<BR>carried out, results OK.<BR>the residual pressures in left leg are checked,<BR>OK. It is verified the accumulators Sys Blue<BR>OK. Cleaned transmitters 3GK1 and 3GK2.<BR>Sys Test to BSCU from MCDU carried out.<BR>The message in ECAM disappears.<BR>885) started with a built-in test of the BSCU, which was the corrective action taken by<BR>the maintenance personnel in most of the reported cases, with results OK. According<BR>to the tasks, the BITE test would act as a confirmation of the real nature of the residual<BR>pressure.<BR>This TFU was closed in August 2003, once the Service Bulletins A340-32-4187 and A-<BR>340-32-4193 were issued by Airbus to solve the problem of spurious indication.<BR>The manufacturer also issued the FOT 999.0030/002 «BSCU Reset subsequent to a<BR>brakes residual braking» dated 19-04-2002 in which the spurious messages of residual<BR>pressure were described and the need to make a reset of the BSCU was mentioned.<BR>The different documents issued by Airbus before the incident were due to a history of<BR>residual braking indications, that, as previously mentioned and among other aircraft,<BR>affected to A-340 EC-GUP also operated by IBERIA. Within 1-11-2001 and 23-11-2001<BR>there were several reports on that aircraft involving residual pressure indications, both<BR>on ground and in flight. Those reports were reported to Airbus, which worked closely<BR>with Iberia to try to solve the issue. A lot of communications took place at and after<BR>those dates between Iberia and Airbus. Several troubleshooting procedures were proposed<BR>and several components were replaced on EC-GUP until the problem finally disappeared.<BR>The manufacturer stated that Iberia had never formally informed them of the results of<BR>the recommended troubleshooting actions of EC-GUP.<BR>Furthermore, the manufacturer added that TSM task 32-40-00-810-927, which is named<BR>«Brakes alternate system has residual pressure in the left MLG», should have been<BR>applied at since the beginning after the five reports in June 2002. They said that TSM<BR>task requests the replacement of the master cylinder if the fault cannot be reproduced<BR>on ground.<BR>The entry points for this TSM task were analysed by the manufacturer after the incident<BR>and they provided evidence that several of the clues present during the squawks in June,<BR>like the «BRAKES RESIDUAL BRAKING» caution, the displayed amber bars, or the CMS<BR>fault message «MASTER CYL L(5422GG)/DUAL VALVE (5403GG)» would have led to the<BR>mentioned task 32-40-00-810-927.<BR>This task consists of the following actions as applicable to the present incident:<BR>« .../... (other text)<BR>3. Fault confirmation.<BR>Technical report IN-062/2002<BR>22<BR>A. Test.<BR>(1) On the panel 117VU, put the parking brake to OFF.<BR>(2) If the lower left indicator of the triple pressure indicator (2GK) shows a pressure,<BR>depressurize:<BR>— The Blue Hydraulic system<BR>— The reservoir of the Blue Hydraulic system<BR>— The Park Brake accumulators<BR>4. Fault isolation<BR>A. Procedure<BR>(1) If the lower left indicator of the triple pressure indicator (2GK) shows a pressure:<BR>replace the PRESS XDCR-BRAKE, BLUE L.../...(otro texto)<BR>B. Procedure<BR>(1) If the lower left indicator of the triple pressure indicator (2GK) does not show<BR>a pressure: replace the MASTER CYLINDER-ALTN BRK L, CKPT (5422GG)<BR>(2) If the fault continues: replace the DUAL VALVE-ALTN BRK.../...(other text).<BR>(3) If the fault continues: replace the FILTER-LP, B RSVR.../...(other text)<BR>C. Test<BR>(1) Do an operational test of the alternate brake system (Ref. AMM Task 32-43-<BR>00-710-801)»<BR>The TSM introduction explained on pages 8 and 10 the meaning of «Fault confirmation<BR>» in case of «Permanent fault» and «Intermittent fault».<BR>In the first case, the «fault is confirmed on ground by performing the test required in<BR>the fault confirmation paragraph. Consequently, the procedure must be applied to troubleshoot<BR>the aircraft».<BR>In the case of an «intermittent fault», specific instructions are provided as follows:<BR>«The fault is not confirmed on ground by performing the test required in the fault<BR>confirmation paragraph. Faults are sometimes generated by electrical transients or<BR>similar events without the aircraft system being faulty. If the confirmation test result<BR>is “TEST OK” or equivalent, no further action is required (unless specified in the fault<BR>isolation procedure). The aircraft may be dispatched. It is recalled that the TSM has<BR>23<BR>Technical report IN-062/2002<BR>been designed to isolate/troubleshoot hard faults. However depending on the airlines<BR>organization, the following can be applied “to trap” intermittent faults:<BR>— if test OK (fault not confirmed) dispatch the aircraft, then perform a monitoring<BR>of the reported symptom on the following flights by checking:<BR>– the previous leg reports<BR>– the PFR/Previous PFRs (if available)<BR>– the log book of the previous flights<BR>after 3 occurrences of the same phenomenon (even through the test still OK),<BR>the other steps of the TSM procedure shall be followed and the LRU involved<BR>be removed. (other text).<BR>— if test NOT OK (fault confirmed), apply the trouble shooting procedure.»<BR>The manufacturer was consulted regarding the practical way of carrying out the task<BR>-927 in this case, and they answered that, because of that «intermittent failure concept<BR>», the -927 procedure should have been applied completely, including the replacement<BR>of the master cylinder on the 9th of June 2002 (after the third squawk). The maintenance<BR>personnel of the operator had a different interpretation because they seemed<BR>not to be applying the intermittent failure part of the TSM, and they said that if there<BR>is no pressure in the triple indicator at the beginning, there is no «Fault confirmation»<BR>and therefore the task ends. They added, late in the investigation process (see above),<BR>that even though this fault confirmation failed because they checked the pressure in left<BR>leg on 11 June 2002, they still applied the operational test 32-43-00-710-801 to be sure<BR>that the system was OK.<BR>1.7. Meteorological information<BR>The METAR at Madrid-Barajas Airport on 7-9-2002 at 13:00 UTC was:<BR>LEMD 071300Z 23011 KT 180V250 9999 FEW080 SCT150 27/07 Q1016 NOSIG<BR>The information gathered shows that the temperature of the atmosphere in the province<BR>of Madrid at 13000 ft of altitude approximately matched that of the International<BR>Standard Atmosphere (ISA).<BR>1.8. Aids to navigation<BR>They do not affect the circumstances of this incident.<BR>Technical report IN-062/2002<BR>24<BR>1.9. Communications<BR>The communications worked normally all the time during the incident. The relevant<BR>communications of the conversations with the control towers of Tenerife Norte and<BR>Madrid-Barajas has been reproduced in other parts of this report.<BR>1.10. Aerodrome information<BR>1.10.1. Airport of Tenerife Norte<BR>This airport has an asphalt runway, 12-30 of 3400 × 45 m. The runway stripe has<BR>3520 × 300 m.<BR>The aerodrome category for rescue and fire fighting is 8 (aircraft of less than 61 m of<BR>total length and 7 m of maximum fuselage width).<BR>1.10.2. Airport of Madrid-Barajas<BR>The airport has three asphalt runways: 33-15 (4100 × 60 m), 36R-18L (3700 × 45 m)<BR>and 36L-18R (4350 × 60 m). The runway stripe has a width of 300 m in all of them.<BR>The aerodrome category for rescue and fire fighting is 9 (aircraft of less than 76 m of<BR>total length and 7 m of maximum fuselage width).<BR>The day of the incident runway 33 was being used for landings and runway 36L for<BR>takeoffs. As a consequence of the incident, when runway 33 remained out of service,<BR>runway 36R was open for landings.<BR>1.11. Flight recorders<BR>1.11.1. Cockpit voice recorder<BR>The aircraft had a solid state cockpit voice recorder (SSCVR) Honeywell P/N 980-6022-<BR>001; S/N 6393705700, that is able to record the latest 120 minutes of the voices and<BR>sounds in the cockpit in four channels. Channel 1 records the sound of the headphones<BR>and boom microphone in the pilot in command position; channel 2 records the<BR>sound of the headphones and boom microphone of the copilot position; channel 3 the<BR>sound of the headphones and boom microphone of the flight observer position; and<BR>channel 4 the cockpit environment sounds through the area microphone.<BR>25<BR>Technical report IN-062/2002<BR>The recorder starts recording since the moment the first engine is started, and keeps<BR>continuously recording the sound of the four channels until five minutes after the last<BR>engine has been shut down. It can also operate in manual mode on ground.<BR>The files corresponding to the 4 channels were downloaded and the sound could be<BR>reproduced with a good quality and made it possible to identify the text of almost all<BR>the conversations between the pilots and communications with the ATC.<BR>Each channel had 2 h, 1 minute and 10 s of sound. Part of the flight from Tenerife Norte<BR>to Madrid had been recorded, exactly 1:21:29 (81 minutes and 29 seconds) elapsed<BR>before the aircraft stopped on runway 33 of Barajas, and then continued recording for<BR>11 minutes and 54 seconds until the recording stopped because the engines were shut<BR>down. Then, a new recording period started with duration of 28 min and 5 s in which<BR>it could be heard the voices of maintenance personnel working inside the cockpit after<BR>the incident.<BR>Therefore, the moments previous and later the incident itself were recorded and the<BR>pertinent information provided by the conversations and other sounds has been used in<BR>several parts of this report.<BR>1.11.2. Flight data recorder<BR>The aircraft was equipped by a digital flight data recorder (DFDR) able to record the<BR>latest 25 h of a total of 663 parameters of the aircraft. The reading of this DFDR was<BR>carried out without problems in a laboratory with capacity for it and the relevant information<BR>provided by the different parameters has been reproduced in several parts of<BR>this report.<BR>The DFDR also showed the following actions of the flight crew:<BR>— During the cruise flight to Madrid the pages of ECAM were not deployed to check<BR>the status of the different systems.<BR>— The spoilers were not armed during the landing in Madrid.<BR>1.12. Wreckage and impact information<BR>The aircraft came to a stop besides the left side of runway 33, with its longitudinal axis<BR>rotated around 10° with respect to the runway axis and with all its wheels on the<BR>asphalt area.<BR>Technical report IN-062/2002<BR>26<BR>The left MLG leg was beyond the runway edge lighting line, and remained approximately<BR>at 5 m from the runway shoulder end, that is, at 40 m from the axis of runway 33,<BR>that has 60 m of total width (distance between the white lines of runway edges), and<BR>at 146 m from the axis of the taxiway J-1. The nose landing gear also remained at<BR>approximately 5 m from the runway shoulder end and at approximately 120 m from<BR>the axis of taxiway J-1.<BR>Therefore, that left MLG leg remained at 313 from the intersection of the axes of runways<BR>33-15 and 36R-18L.<BR>When the runway could be inspected, it was noticed that starting in the point the aircraft<BR>had stopped and coming back in the sense towards the threshold of runway 33<BR>(i.e. going in the sense contrary to the movement of the aircraft during the landing roll),<BR>tracks of the wheels of the left and right MLG legs could be clearly noted. The tracks<BR>consisted of eight dark lines that corresponded to the sides of the tires showing that all<BR>the wheels had burst. At 60 m form the point where it was stopped, the track of the<BR>left leg crossed the runway edge lighting line (at 2 m from the next runway edge light),<BR>and 60 m backwards it crossed the white line of the runway side stripe. During the previous<BR>60 m it could be seen that the wheel rims number 1 and 5 (both outboard wheels<BR>of the left leg) had dragged along the runway, although no appreciable grooves or<BR>other damage to the runway surface was noticed.<BR>At 240 m from the point it finally stopped (i.e., at 73 m from the intersection of runway<BR>36R), the tracks of the right MLG leg disappeared at a point located 8.2 m to the<BR>left of the runway axis.<BR>The tracks of the left leg continued being visible going backwards, they crossed the<BR>intersection of runway 36R and started softening and blurring being confused with the<BR>tracks of other aircraft 630 m aft of the point where the aircraft stopped (i.e. at 900 m<BR>from the threshold of runway 33).<BR>The damage to the aircraft consisted of the burst of the eight wheels of the left and<BR>right legs and damage to the brake assemblies number 1, 5 and 6 with the following<BR>description:<BR>Wheels 1, 2, 5 and 6 showed heavy rubbing with loss of material of the rim and tire<BR>burst, due to friction with the runway.<BR>Wheel 3 had friction in the rim and tire burst due to contact with the runway.<BR>Wheel 4 had friction in the rim with loss of material and tire burst due to friction with<BR>the runway.<BR>Wheels 7 and 8 showed tire burst due to friction with the runway but the rims did not<BR>have noticeable damage.<BR>27<BR>Technical report IN-062/2002<BR>Figure 6. Wheels 3, 4, 7 y 8 (right leg; seen from the rear right angle) after the aircraft stopped<BR>on the runway. The white line is the runway side stripe marking of 33. Note the two narrow<BR>tracks of every wheel after they burst<BR>The brake assemblies 1, 5 y 6 showed heavy rubbing with loss of material in the fitting<BR>and in the brake disks, due to friction with the runway.<BR>When the aircraft was inspected in a hangar, there were no signs of fire having affected<BR>the landing gear. The lower part of the wing and the inboard flaps did not show<BR>any traces of smoke.<BR>The maintenance personnel of the operator replaced the wheels of the aircraft on the<BR>runway and then the aircraft was towed to a hangar.<BR>1.13. Medical and pathological information<BR>There were no personal damages during the event.<BR>Technical report IN-062/2002<BR>28<BR>1.14. Fire<BR>At Tenerife Norte Airport there was no fire, although there was smoke coming out the<BR>wheels due to the high temperature reached by the brakes.<BR>At Madrid-Barajas Airport, a lot of smoke was seen from the tower immediately after<BR>the incident. Another aircraft said on the radio that EC-IDF had fire on the wheels. The<BR>fire fighters were advised by the tower around 13:06 h, and at 13:09:45 h the crew<BR>confirmed to the tower that they were around the aircraft. At 13:09:55 h, the tower<BR>had already received confirmation from the fire fighting crew that the fire was extinguished.<BR>According to their report, the fire fighters, which had been warned by the tower, reached<BR>the area of the incident and found all the wheels in fire, and they positioned<BR>around the aircraft and quickly extinguished the fire and then continued cooling the<BR>gears. They used a total of 250 kg of chemical powder and 1750 l of foam, although<BR>this later figure was higher than the amount normally needed due to the malfunction<BR>of one of the extinguishing vehicles.<BR>According to some information gathered later on, the flames were clearly visible from<BR>the area of the south tower of the airport. However, when the aircraft was inspected<BR>in a hangar, there were no rests of combustion in any part in the wheel area.<BR>1.15. Survival<BR>There were no accelerations of such a high magnitude as to produce impacts in the passenger<BR>cabin. An emergency evacuation was not commanded, and the passengers left<BR>the aircraft in a normal way using air stairs provided to the aircraft and were taken to<BR>the airport with shuttle coaches.<BR>1.16. Tests and research<BR>1.16.1. Ground test to locate the problem<BR>After the incident, the specialists of the manufacturer proposed to carry out a functional<BR>check of the brake system of the aircraft following a test plan outlined in the «Technical<BR>Disposition» of Airbus Ref. TD/B/2002/0341 (Issue 2), that basically consisted of<BR>trying to reproduce the residual pressure in the alternate system through the use of the<BR>pedals and the parking brake. If the residual pressure was not reproduced, then the flow<BR>rate during the bleeding of the left and right low pressure lines (between the BDDV and<BR>the master cylinders) should be measured to look for restriction points in the circuit. The<BR>details of the contents of the Technical Disposition are included in Appendix B. This pro-<BR>29<BR>Technical report IN-062/2002<BR>cedure was not a part of the previous maintenance documentation of the aircraft. It<BR>was specifically prepared for the occasion after several weeks of work of the specialists<BR>of the manufacturer.<BR>The test was carried out and it was found that the failure produced during the incident<BR>could not be reproduced, but the flow rate measurement showed that there was no<BR>flow in the left low pressure circuit while the flow in the right circuit was 50 cl in 20 s.<BR>This meant that there was no way for the return flow from chamber C1 to chamber C2<BR>through the left master cylinder (see Figure 4), that is, that there was no “dead band”<BR>and the pressure was trapped inside chamber C1 even when the pedal was not pressed<BR>at all.<BR>This could be due to one of the two following factors:<BR>a) The master cylinder was defective, with a length longer than the 170 mm specified,<BR>in such a way that is should be compressed when assembled in the aircraft, producing<BR>the closure of the valve.<BR>b) The rigging of the left pedal was defective, in such a way that the cylinder, even<BR>having the correct length, had still to be compressed during assembly, again producing<BR>the already mentioned closure of the valve.<BR>The master cylinder P/N C 24592020 (Functional Item Number 5422GG), S/N H2121 was<BR>replaced by other master cylinder off the shelf and the flow rate test was done again,<BR>and this time a flow of 50 cl in 25 s was obtained. With this result, the specialists of<BR>the manufacturer confirmed that the master cylinder was defective and was the component<BR>producing the residual pressure. Pedal rigging pins were installed to confirm<BR>correct rigging of the pedals.<BR>The master cylinder was sent to its vendor-manufacturer, Messier-Bugatti, for a detailed<BR>inspection and teardown.<BR>1.16.2. Release to service of the aircraft<BR>After the replacement of the master cylinder mentioned in the previous paragraph, the<BR>specialists of the aircraft manufacturer issued the Trouble Shooting Report N°<BR>3048/SEE32/TSR/1002 that confirmed that «the original master cylinder was faulty and<BR>was the sole cause of the residual braking behaviour. Also, it is confirmed that the pedal<BR>rigging is satisfactory». Although not specifically required by the manufacturer specialists,<BR>the operator carried out a flight test and it was noticed that after some time most<BR>of the pressure of the alternate brake system was lost, while the normal system functioned<BR>correctly.<BR>Technical report IN-062/2002<BR>30<BR>Then the BDDV P/N 5403GG S/N H2718 was replaced and the brake system carefully<BR>purged. A new flight test showed that both brake systems functioned correctly and the<BR>aircraft was returned to service.<BR>The replaced dual valve was also sent to Messier-Bugatti for additional inspection.<BR>1.16.3. Inspection of the master cylinder S/N H2121<BR>The master cylinder disassembled from aircraft EC-IDF after the incident was subject to<BR>several tests at the facilities of its manufacturer in Molsheim (France). The cylinder had<BR>been sent in a sealed package and it was intended to retain as much hydraulic fluid inside<BR>as possible.<BR>The tests carried out were the following:<BR>— Dimensional measurement: The length was 170.31 mm (the nominal value is between<BR>170.050 and 170.100 mm). The «dead travel» was 0.58 mm (the nominal<BR>value was between 0.4 y 0.5 mm). The total travel was 21.68 mm (the specified<BR>value is 20.5 to 22.3 mm).<BR>— Hydraulic fluid: the master cylinder was empty. It was not possible to recover hydraulic<BR>fluid for its analysis.<BR>— Operational test: The graph load vs. travel was prepared according to the Component<BR>Maintenance Manual (CMM). It was observed that the results were outside<BR>tolerances in a series of points both in load (compression) and extension of the cylinder.<BR>For instance: with 10 mm of travel in load the force should be between 139<BR>Nw and 153 Nw; the measured value was 162 Nw (7% above the specified limit).<BR>— It was made a flow rate test under pressure. For that purpose, with the port B open,<BR>a pressure of 2.4 bar was applied to port A and the flow vs. travel of the cylinder<BR>was measured. In compression there was a flow of 2.17 l/min when there was no<BR>travel and the value of the flow was being lower. With 0.33 mm the flow was 0.01<BR>l/min and with 0.34 mm there was no flow anymore. In unload of the cylinder there<BR>was no flow with 2 mm of travel, and the travel was reduced up to the moment<BR>that with 0.36 mm the flow started being 0.01 l/min.<BR>— The cylinder was disassembled and no noticeable defects were found. The different<BR>subcomponents were dimensionally checked and all of them were found inside tolerances<BR>except the «small» spring or spring valve (spring R1) that reached the nominal<BR>length with a load of 4 Nw instead of the 5 Nw of the specification. The specialists<BR>in the system considered this difference was not significant. The preformed<BR>packing of the valve was deformed because of the contact with the valve, and had<BR>no longer the squared section with which it was manufactured.<BR>The cylinder was assembled again and it was adjusted in such a way that the length<BR>and the dead travel were the same as previously, and the operational and flow rate tests<BR>31<BR>Technical report IN-062/2002<BR>were carried out again. The master cylinder was now inside specified limits during compression,<BR>but it was still slightly outside tolerances during the extension. A possible<BR>explanation for this behaviour was that some minute particles that were producing a lot<BR>of friction inside the cylinder could have been eliminated during the disassembly and reassembly.<BR>After this test the length was measured again and it had increased up to<BR>170.35 mm. The dead travel had decreased from the previous 0.58 mm to 0.48 mm,<BR>and no clear explanation was obtained for this fact. The flow rate test provided the<BR>same results as previously.<BR>Messier-Bugatti informed that those cylinders are manufactured by a subcontractor. The<BR>S/N H2121 passed its quality control after manufacture on 13-6-2000, and it was then<BR>recorded a dead travel of 0.44 mm (inside limits) and a total travel of 21.90 mm (inside<BR>limits), with the diagram load-travel inside tolerances. However, the length of the<BR>cylinder was not recorded during quality control acceptance tests at that time. Messier-<BR>Bugatti informed that «The unit is adjusted during assembly».<BR>The acceptance test did not include a flow rate test under pressure.<BR>Information gathered from technicians of the manufacturer indicated that they had<BR>never seen a cylinder with a length above specifications.<BR>The master cylinder was reserved for further investigation at the facilities of Airbus in<BR>Filton (United Kingdom). See paragraph 1.16.5.<BR>It was requested to Messier-Bugatti to provide an analysis of all the information<BR>retrieved during the tests in order to establish a hypothesis of the circumstances or<BR>the subcomponent of the master cylinder that made its length to be outside tolerances<BR>and that ultimately produced residual pressure in the alternate system of the<BR>A-340 EC-IDF.<BR>Messier-Bugatti never provided a detailed analysis, but answered through an E-mail on<BR>12-9-2003 that no subcomponent of the cylinder had been identified as defective, and<BR>that in December 2002 they had modified their procedures to include a systematic measurement<BR>of the length of every cylinder after manufacture. They also added that<BR>«remains a doubt as to the possible implication of other parts such as brake pedal<BR>assembly».<BR>1.16.4. Inspection of the dual valve (BDDV) S/N H2718<BR>The dual valve was disassembled from EC-IDF following a flight test carried out after<BR>the incident. It was subject to several tests at the facilities of its manufacturer Messier-<BR>Bugatti in Molsheim (France). The valve had been sent in a sealed package and it was<BR>Technical report IN-062/2002<BR>32<BR>intended to keep inside as much hydraulic fluid as possible. However, the package was<BR>opened at Messier-Bugatti and only 1 ml of liquid could be collected.<BR>The recovered fluid was observed in the microscope by specialists of the manufacturer<BR>of the component, who indicated that it contained some metal particles between 15<BR>and 80 microns. There was not enough liquid to carry out a more complete analysis.<BR>A functional test was performed in accordance with CMM 32-43-16, which includes a<BR>«Proces Velbal d’Essai» (test plan). All the results of this analysis were found inside tolerances.<BR>Messier-Bugatti stated that the valve was in normal operating conditions and<BR>was released as far as the investigation was concerned.<BR>1.16.5. Additional testing of the master cylinder S/N H2121<BR>The cylinder was sent to the facilities of Airbus in Filton (United Kingdom) to be put into<BR>a test bed to simulate the actual conditions of a flight of aircraft EC-IDF. The temperature<BR>changes that appear in climb, cruise and descent were considered as a main factor<BR>leading to the build-up of residual pressure in the alternate brake system.<BR>Airbus carried out additional testing, but, even though the test conditions were more<BR>stringent, it was no longer possible to reproduce the residual pressure. However, because<BR>the cylinder had already been disassembled (see 1.16.3), the feasibility of those results<BR>was doubtful and had anyway to be analysed. It was concluded that, after disassembly,<BR>the master cylinder was no longer «the same» as during the incident. Therefore, no conclusion<BR>could be drawn from the additional testing.<BR>1.16.6. Inspection of the pedal cover<BR>Time after the investigations on the master cylinder took place, the pedal cover that was<BR>installed on EC-IDF upon delivery was pointed out as a possible cause of residual pressure.<BR>Therefore, an inspection for scratches and marks was carried out on that cover<BR>several months after the incident. The main function of that cover was to avoid that<BR>some foreign objects as pocked calculators or pens could fall to the brake assemblies.<BR>The results of the inspection were:<BR>1. There was no chaffing or scratching present on the MSN474 pedal assemblies covers.<BR>2. All clearances between the pedal assemblies and their covers were sufficient to<BR>allow normal operation.<BR>3. The operation of the pedal assemblies during braking inputs was normal.<BR>33<BR>Technical report IN-062/2002<BR>4. The marks seen on the master cylinders of EC-IDF did not indicate any abnormality.<BR>1.17. Organizational and management information<BR>1.17.1. Technical flight records of the aircraft<BR>On board the aircraft there should always be a block of forms of the aircraft flight logbook.<BR>Each form triplicates in 3 pages, from which the last (page 3/3, yellow colour)<BR>must always remain attached to the block. In the right upper area of the form there is<BR>a square titled «Capt. Acceptance» with a space for the signature of the pilot in command<BR>of the aircraft. There is a column called «Complaints» («Anormalidades») to be<BR>filled up by the crew, other called «Maintenance Actions» («Correcciones») to be filled<BR>by the maintenance personnel and other column of signatures of the maintenance personnel<BR>that have handled the complaints reported by the crew. The result of that handling<BR>may be «Fixed», «Under observation» or «Deferred».<BR>The Basic Operations Manual prepared by the operator (revised on 26-5-2002), in<BR>paragraph 8.1.11, gives instructions to the flight crews to fill in the flight logbook<BR>forms, that basically are «All the required data in the form must be carefully completed<BR>». It is also stated that: «In the spaces reserved for the signature it is necessary no<BR>only sign, but to provide the identification number. The captain will sign the square of<BR>aircraft acceptance of the form corresponding to the flight that is going to be carried<BR>out. In this way, he will record the acknowledgment of the corresponding inspections,<BR>as reflected on page 3/3 of the previous flight logbook, and of the abnormalities and<BR>maintenance actions that are also written in this page 3/3 of the previous flight. This<BR>signature of the captain will also serve as confirmation of the complaints and data<BR>recorded during his flight. In the event there are no complaints, the word “NIL” will<BR>be written».<BR>The «Manual de Procedimientos de Mantenimiento en red» («Maintenance Procedures<BR>Manual») of the operator (Section 2, Revision 7 of 18-6-02) also provides guidance for<BR>the handling and completion of the flight logbook pages. It is mentioned that the maintenance<BR>action after the reported complaints must always be done in accordance with<BR>the established documentation and, in the event that maintenance action or repair is<BR>not included in the documentation, the corresponding instructions will be consulted to<BR>the corresponding Engineering Support Department, and this circumstance will be reported<BR>in the flight logbook.<BR>The MOE-145 («Maintenance Organization Exposition») and the “Manual de Procedimientos<BR>de Mantenimiento en red” (Section 2, Revision 7) contain instructions for the<BR>treatment of the flight logbooks by the line maintenance personnel and the transit inspections<BR>of the aircraft. It is stated that in the event the ground personnel find an<BR>Technical report IN-062/2002<BR>34<BR>abnormality during their line inspection, even though it was not reported by the crew,<BR>they must record it in the column of «Maintenance Actions» of the logbook. In the description<BR>of the maintenance action reference to the corresponding part of the Maintenance<BR>Manual must be done.<BR>In summary, the crew must review the logbook of the previous flight and the captain<BR>must sing the aircraft’s acceptance in the logbook page of the actual flight<BR>been prepared, and this will show that he is aware of the disposition of the previous<BR>complaints. The signature will also validate the new complaints noted during<BR>his flight, whose maintenance actions will be accepted by the captain of the next<BR>flight, and so on.<BR>1.18. Additional information<BR>1.18.1. Telex to the operators issued by Airbus Industrie<BR>On 31-10-2002 Airbus issued an «Operators Information Telex» in which the operators<BR>were informed of aircraft A319, A320, A321, A300, A300-600, A310, A330 and A340<BR>of the circumstances of the event happened on 7-9-2002, and of the actions to be<BR>carried out by the crews in the event they noticed residual pressure in flight. The Telex<BR>said that in this case:<BR>«AS USUAL, THE NORMAL BRAKING AND ANTISKID SYSTEMS HAVE TO BE USED,<BR>AND THIS EXPLAINS WHY THERE IS NO ECAM/FCOM PROCEDURE EXCEPT . IN ADDITION, USING THE AUTOBRAKE (AS RECOMMENDED<BR>IN THE SOP) PREVENTS ASYMMETRICAL BRAKING DUE TO RESIDUAL BRAKING<BR>PRESSURE IN THE ALTERNATE BRAKING SYSTEM, SINCE ALTERNATE PRESSURE IS<BR>NOT SUPPLIED TO THE BRAKES WHEN NORMAL BRAKING IS ACTIVE.<BR>HOWEVER, IN THE LIGHT OF THE REPORTED EVENT, AIRBUS WILL PUBLISH SOME<BR>RECOMMENDATIONS FOR ALL AIRCRAFT, IN THE FCOM STANDARD OPERATING<BR>PROCEDURES’ “APPROACH PHASE”, TO AVOID SWITCHING OFF THE ANTISKID<BR>AND NOSEWHEEL STEERING FUNCTION, AND POSSIBLY TO ELIMINATE ALTERNATE<BR>RESIDUAL BRAKING PRESSURE.<BR>A330/A340 RECOMMENDATIONS DIFFER SLIGHTLY FROM THOSE OF THE OTHER<BR>AIRCRAFT TYPES, SINCE RESIDUAL BRAKING (FROM THE NORMAL OR ALTERNATE<BR>BRAKING SYSTEM) IS DISPLAYED ON THEIR ECAM WHEEL PAGE. ON OTHER AIRCRAFT<BR>TYPES, ONLY RESIDUAL BRAKING ON THE ALTERNATE SYSTEM IS VISIBLE,<BR>AND IS DISPLAYED ON THE TRIPLE INDICATOR.<BR>FOR A330/A340 AIRCRAFT (NOT APPLICABLE TO A340-500/600):<BR>35<BR>Technical report IN-062/2002<BR>WHEN THE LANDING GEAR IS DOWN:<BR>– ECAM WHEEL PAGE CHECK<BR>– THE ECAM WHEEL PAGE APPEARS BELOW 800 FEET, OR AT LANDING GEAR<BR>EXTENSION.<BR>– CHECK FOR THREE (A330), OR FOUR (A340) LANDING GEAR GREEN INDICATIONS.<BR>– IF RESIDUAL PRESSURE IS INDICATED, PRESS THE BRAKE PEDALS SEVERAL TIMES.<BR>SELECT “AUTO BRK MED”. IF RESIDUAL PRESSURE REMAINS:<BR>– BEWARE OF POSSIBLE BRAKING ASYMMETRY AFTER TOUCHDOWN, WHICH<BR>CAN BE CONTROLLED USING PEDALS.<BR>– DO NOT SWITCH OFF THE A/SKID & NWS: THE ANTISKID FUNCTION LIMITS<BR>THE EFFECT OF RESIDUAL BRAKING, AND PREVENTS TIREBURST.»<BR>Additionally, Airbus modified the «Standard Operating Procedures», paragraph 3.03.19<BR>of the «Flight Crew Operating Manual» (FCOM) to include the relevant information of<BR>the telex.<BR>Before the incident, those recommendations were not included in any Airbus document.<BR>1.18.2. History of similar cases<BR>The manufacturer of the aircraft informed that they were aware of several cases of brake<BR>residual pressure in flight, and that it was known that most of those indications were<BR>spurious (see paragraph 1.6.3 with mention to the TFU issued to cover the matter). No<BR>failure of the brake system detected in flight had produced an incident that ended in<BR>tire burst during landing.<BR>The operator informed (see 1.6.3) that in year 2001 there was a long period during<BR>which aircraft EC-GUP was affected by residual pressure, and they worked with Airbus<BR>to solve the problem.<BR>1.18.3. Other safety actions carried out by the manufacture of the aircraft<BR>In addition to the telex mentioned in 1.18.1, the manufacturer started a revision of their<BR>procedures of testing the brake system at the end of the assembly line and modified<BR>parts of the maintenance manual associated to the master cylinder.<BR>Technical report IN-062/2002<BR>36<BR>They also started the study of a modification to the design of the master cylinder to<BR>avoid that environmental factors could produce the appearance of residual pressure in<BR>the brake system.<BR>1.19. Useful or effective investigation techniques<BR>None.<BR>37<BR>Technical report IN-062/2002<BR>2. ANALYSIS<BR>2.1. Operation during the Madrid-Tenerife flight<BR>When the landing gear was lowered during the descent to Tenerife the crew observed<BR>in the WHEEL page of the ECAM that the 24 bars that represent the brakes of the wheels<BR>of the left MLG were lit in amber colour, indicating that there was pressure trapped.<BR>Under those conditions, they did not check the triple indicator located in the central<BR>panel of the cockpit, which would have allow them to note that the pressure was in<BR>the left alternate system, not in the normal system.<BR>Anyway, although the information recovered suggest that the crew did not recognize<BR>the origin and possible effects of the problem and they thought there was a «spurious<BR>indication», they made the right decision of landing with the antiskid connected, which<BR>was correct, and without autobrake, as they were used to do in occasions at the discretion<BR>of the captain.<BR>However, they decided to retard the application of brakes to prevent possible braking<BR>problems in the event there really was a malfunction of the systems, instead of an indication<BR>failure as they suspected. The result of this decision was that during the time the<BR>brake pedals were not pressed, the alternate system was still active and, therefore, the<BR>900 PSI of residual pressure that were present were transmitted to the left wheels, and<BR>the aircraft started deviating towards that side. At the moment of touchdown there<BR>were several pressure releases in the left brakes commanded by the antiskid system<BR>intermittently, and the wheels did not burst.<BR>The copilot, that was the PF during the landing, applied right rudder as coherent with<BR>his intention to delay the brake application, until the deviation was very important, and<BR>the aircraft approached up to 8 m to the left edge of runway 12 and a decrease in the<BR>effectiveness of the rudder was noted as the speed was reducing. At those moments,<BR>he applied heavily right brake and also left pedal, until the aircraft deviated to the right<BR>of the runway axis and came to a stop. The right pedal application started when the<BR>aircraft had between 60 kt and 70 kt of ground speed, and reached its maximum value<BR>when the speed was 50 kt.<BR>At the moment of pedal application, the green or normal system was activated and the<BR>residual pressure of the alternate system fell to 0 psi. However, when the speed was<BR>below 80 kt the pedals had not yet been pressed and there was still a pressure of 900<BR>psi and, when the inhibition of the caution of «brakes residual braking» ended, this caution<BR>was displayed in the ECAM (see paragraph 1.6.4.4).<BR>The result of those circumstances was that the crew was surprised by the behaviour of<BR>the aircraft, and they thought there had been a malfunction in the brake system that<BR>39<BR>Technical report IN-062/2002<BR>remained during the landing roll, and that the brakes heated until the corresponding<BR>ECAM warning was displayed. However, the presence of the antiskid allowed an effective<BR>braking action and avoided the burst of the tires.<BR>Once they had vacated the runway, the crew reset the BSCU. If at those moments they<BR>had checked the triple indicator or the ECAM wheel page, they would have noted that<BR>the residual pressure had disappeared, and therefore that action, required by the Operations<BR>Manual of the operator if the caution appears on ground, was not needed. The<BR>procedures of the manufacturer indicate in one chapter that maintenance action is<BR>required if the caution is noticed at engine start or during taxi, and in other chapter<BR>(«Supplementary techniques» 3.04.32 P1) that the crew may reset the BSCU. That<BR>applies when the aircraft is on ground.<BR>2.2. Maintenance actions in Tenerife Norte<BR>When the aircraft was parked in the apron, the crew commented with the maintenance<BR>personnel the circumstances they had faced during the landing. At those moments,<BR>the immediate problem they had was a high brake temperature, which was cooled with<BR>fans.<BR>From the information gathered it could be concluded that the ground maintenance personnel<BR>was fully aware of the problem of residual pressure that had to be handled<BR>during the previous descent and landing. They actually saw the «Post-Flight Report» provided<BR>by the aircraft that had recorded that the caution «Brakes Residual Braking» had<BR>appeared at 9:12 h in the phase «Cruise 06». This caution was not displayed to the<BR>crew at those moments, because it is inhibited. During the landing roll, below 80 kt,<BR>the warning was displayed at around 9:22 h when the inhibition ended.<BR>However, the flight crew had not recorded any complaint or squawk in the flight logbook,<BR>neither the residual pressure appearance, nor the deviation during the landing<BR>roll, nor the high brake temperature.<BR>The ground personnel took action to determine the origin of residual pressure, but did<BR>not write anything in the logbook. The maintenance procedures indicate that if the<BR>ground personnel detect any malfunction, they must write it down even when not previously<BR>reported by the flight crew.<BR>Afterwards, the data gathered suggest that while the line maintenance personnel was<BR>trying to contact another department of the operator to seek support information to<BR>treat the problem of residual pressure, the boarding of the passengers started for the<BR>flight back to Madrid. This fact probably produced additional stress regarding the<BR>need to dispatch the aircraft as soon as possible. Anyway, given the facts that the<BR>residual pressure had disappeared and that the support personnel in Barajas could not<BR>Technical report IN-062/2002<BR>40<BR>be contacted, the «transit check performed» box of the logbook was completed and,<BR>since there was not any complaint recorded in the logbook, theoretically there was<BR>also nothing to correct, and the doors were closed and the pilot in command decided<BR>to initiate the flight, with the understanding, according to his statement, that the aircraft<BR>was released to service. After the boarding, contact with maintenance people in<BR>Madrid was finally achieved, and the situation was commented but no further maintenance<BR>action was carried out. The maintenance personnel gave additional instructions<BR>to the crew, which in turn had decided that if during taxi any malfunction of the<BR>brake systems was noted, they would return to the parking area for additional maintenance<BR>action.<BR>The captain did not complete the box «Captain Acceptance» («aircraft acceptance by<BR>the captain») of the next page of the logbook that pertained to the flight of the incident.<BR>It is considered that it is possible that some doubts or misunderstandings existed regarding<BR>who had ultimate responsibility over the aircraft at every moment, but it would<BR>have been necessary to make additional efforts to understand with detail the causes and<BR>possible effects of the residual pressure in the brake system. The BSCU test was initiated<BR>but not completed. Therefore, the intended maintenance actions were not finished.<BR>In this case, the facts that the aircraft veered to the left and very high temperatures<BR>were achieved, including smoke coming out from the wheels, should have been sufficient<BR>to remove any doubt about the spurious nature of the fault. It should have been<BR>clear that the residual pressure had been real during the landing and therefore more<BR>troubleshooting was needed.<BR>When the aircraft started taxiing again, the «RESIDUAL BRAKING» caution had disappeared<BR>and the crew did not report problems with the controllability of the aircraft<BR>during the taxi towards the runway and takeoff.<BR>2.3. Operation during the flight Tenerife Norte-Madrid-Barajas<BR>After the doors were closed and the taxi started, the crew came to the conclusion that<BR>the brake system was functioning normally, and proceeded with the takeoff. The landing<BR>gear was left down for some time to cool the brakes that still had a slightly high<BR>temperature. During the return flight to Madrid, the crew had at least two hours to<BR>study the actions to be taken in the event the residual pressure reproduced during the<BR>descent.<BR>The DFDR data show that the pages of the ECAM were not displayed to check the status<BR>of several systems, as required by the Operations Manual (2.01.52, 15-09-200,<BR>«Watch the evolution of the parameters of the engine and aircraft systems though the<BR>ECAM, regularly calling the different pages...»).<BR>41<BR>Technical report IN-062/2002<BR>During the descent to Madrid, the residual pressure in the left side of the alternate<BR>system had started to increase progressively when the aircraft was at 13000 ft.<BR>At 12:58:02 h, the page WHEEL of the ECAM was deployed and the crew detected that<BR>pressure, because they saw in amber colour the 24 bars representing the left brakes.<BR>The reaction of the crew was to reset the BSCU, moving to OFF and then to ON the<BR>switch ANTI SKD & N/W STRG, but the amber bars did not disappear.<BR>Faced with this situation, the crew expressed their concern, because the preceding landing<BR>in Tenerife, where the deviation had been considered to be caused by the malfunction<BR>of some component of the brake system during the landing roll.<BR>The residual pressure continued increasing and 500 psi were reached at the moment in<BR>which the landing gear was lowered, at 12:58:38 h when the aircraft was approximately<BR>at 4000 ft. At that moment, the page WHEEL of the ECAM was automatically<BR>deployed and the aircraft carried out several auto checks of the hydraulic system, and<BR>the normal brake system was momentarily connected and the residual pressure of the<BR>left side released until the checks finished and returned to its previous value.<BR>They carried out another reset «cycle» of the BSCU, for 24 s. This action, carried out<BR>once the landing gear was down, was contrary to the operational procedures of the aircraft,<BR>and was unable to make disappear the amber bars, although they probably disappeared<BR>momentarily while the BSCU switched off and then on.<BR>Should the crew checked and interpreted correctly the triple indicator, they would have<BR>noticed that the residual pressure was in the alternate brake system, which is not controlled<BR>by the BSCU. This could have help conclude that the resets of the BSCU would<BR>not be effective in the build up of residual pressure.<BR>Under those conditions, there was a conversation in the cockpit in which it was said that<BR>one possibility would be to disconnect the antiskid, with the intention, according to the<BR>later statements of the crew, of avoiding that electronic systems not controlled by the pilots<BR>applied or released braking pressure in the uncertain conditions in which the whole system<BR>seemed to be. Finally they disconnected again the switch A/SKID & N/W STRG that was<BR>maintained in that condition for the remainder of the approach and landing. Thus, the possibility<BR>of activating the normal brake system (that had no residual pressure and that would<BR>have been activated at the moment of pressing the brake pedals) was precluded.<BR>The autobrake system was not armed, and anyway it would not have functioned because<BR>the antiskid was disconnected.<BR>The aircraft continued its approach and the crew commented the possible behaviour of<BR>the system during the landing. The conversations indicated that there were certain<BR>Technical report IN-062/2002<BR>42<BR>doubts about the functioning of the brakes in the status they were. The copilot read<BR>the corresponding part of the Operations Manual, reminding clearly that the pressure<BR>should be checked in the brake indicator and that it should not be above 1000 psi any<BR>time, because otherwise the wheels would burst.<BR>Almost simultaneously to the moment the tower authorized the landing in runway 33,<BR>with wind 210° and 10 kt, the crew decided to land close to the threshold of the runway<BR>and use reverse without touching the brakes. At those moments, the «Glide slope<BR>» warning of the GPWS sounded, with the aircraft at 600 ft of radio-altitude. The<BR>PF said that this warning should be disregarded because, according to a later statement,<BR>he wanted to carry out a somewhat low approach to touchdown as soon as<BR>possible.<BR>On the other hand, with the time employed in the revision of the brake system in the<BR>manuals and deciding what to do regarding the residual pressure, it is very probable<BR>that the checklist of final was not read and completed (paragraph 2.01.63 of the Operations<BR>Manual of the operator). One of the consequences of this fact was that the spoilers<BR>were not armed during landing.<BR>There were no special instructions given to the passengers and the tower was not advised<BR>that some abnormality with the brake system could appear, to allow the fire fighters<BR>to take positions with time in advance. As it happened in Tenerife-Norte, at least a<BR>high brake temperature could be expected that even produced smoke at that airport.<BR>Those facts must be regarded as being a part of a situation with high workload and<BR>some uncertainty inside the cockpit. The workload would have been produced by the<BR>mental evaluation of the different malfunction scenarios of the brakes and the corresponding<BR>corrective actions, and the use of the manual, which eventually absorbed most<BR>of the attention of the crew at those final moments of the approach. Even though there<BR>was available time during the cruise flight, the crew was exposed to face the problem,<BR>look up for information and make decisions in the moments previous to the landing,<BR>after having lowered the landing gear.<BR>The aircraft floated for 3 s in the flare until the right and left MLG legs touched down<BR>about 240 m after the threshold of runway 33, at 13:03:27 h. Since the antiskid was<BR>inactive, there was no momentarily release of pressure as it happened during touchdown<BR>in Tenerife. Therefore, when they contacted the runway, the left wheels where<BR>locked and it is probable that they burst soon afterwards.<BR>Approximately 7 s later, the copilot asked whether the aircraft had a tendency to deviate.<BR>The captain and PF answered: «For the moment no», and added two seconds later:<BR>«Yes, it deviates, yes» and then «It departs a little bit». Seven seconds later the captain<BR>told the copilot to apply pedal and then to brake with the right brake. The copilot answered<BR>he was already braking.<BR>43<BR>Technical report IN-062/2002<BR>At 13:03:45 h the right pedal was fully pressed, making the pressure of the alternate<BR>system of that side to increase up to 2500 psi, and the pressure of the left side to<BR>decrease down to 600 psi from the initial 800 psi of trapped pressure built-up during<BR>the flight.<BR>The left pedal was not pressed any time and the aircraft finally came to a stop with all<BR>the wheels burst.<BR>According to some braking marks noted in runway 33 after the incident, the first point<BR>where tracks of the bust left wheels are clearly noticed is 630 m rearwards the point of<BR>final stop of the aircraft (i.e. approximately 900 m away from the threshold of runway<BR>33). This would indicate that initially the aircraft touched down (at 240 m from the<BR>threshold) and the residual pressure of 800 psi that was amassed in flight started actuating<BR>in the left side. To avoid the deviation the PF applied more and more right rudder,<BR>in a scenario similar to that faced in Tenerife, although now the pressure was 800 psi<BR>instead of 900 psi in Tenerife. At a given moment, the left wheels burst because they<BR>had touched down already locked, and from that point in which the aircraft had approximately<BR>100 kt of speed, the directional control was much lesser because of the combination<BR>of decrease of effectiveness of the rudder with the burst of the tires, that<BR>initially decreased the braking force on that side.<BR>The aircraft deviated in that area to the right of the runway axis to move then clearly<BR>to the left starting approximately at 100 m before the intersection with runway 36R.<BR>This fact could be due to the continuous decrease of the effect of the rudder and the<BR>loss of part of the left tires and dragging of the rims and brakes assembly along the<BR>runway surface.<BR>The PF decided to apply right brake and 40 m after crossing runway 36R the right<BR>pedal started to be pressed until it reached its stop when the aircraft was 73 m<BR>beyond the intersection of both runways. In this point, tracks of the right wheels were<BR>first noticed in the runway. These tracks showed a heavy braking action until the right<BR>tires burst because a high pressure up to 2500 psi was applied. That braking action in<BR>the right side prevented the nose of the aircraft moving further to the left of the runway<BR>axis and from that point on the aircraft had a straight trajectory towards the runway<BR>left edge.<BR>The left wheels crossed the runway side stripe marking in a point located 120 m before<BR>the final position of the aircraft, while the right wheel came to a stop just above that<BR>marking (see the white line of Figure 6).<BR>Finally, the braking action (although reduced because of the burst of all the wheels) and<BR>that of the thrust reverses that were deployed after touchdown, allowed the aircraft to<BR>be stopped inside the asphalted zone, although with the left wheels beyond the runway<BR>edge lighting line.<BR>Technical report IN-062/2002<BR>44<BR>2.4. Actions after the aircraft came to a stop<BR>The information gathered indicate that although the fire fighters were not previously<BR>warned, at 13:09:55 h, that is, after 3 min and 55 s the tower activated the alarm, they<BR>had extinguished the fire of the wheels and had the situation under control. It took<BR>some time to the flight crew to receive information from outside the cockpit regarding<BR>the status of the aircraft.<BR>The aircraft stopped at 13:05 h and at 13:05:41 h another aircraft informed by radio<BR>that the wheels were on fire.<BR>Initially, the flight crew were evaluating the need to shut down the engines, advise the<BR>cabin crew to be prepared or to order an evacuation. In the mean time, they called their<BR>company to request assistance. They were seeing fire fighters around the aircraft, but<BR>did not have clues of fire or smoke. At 13:08:24 h they addressed the passengers and<BR>the cabin crew members to advise them to remain seated without using the mobile telephones.<BR>Therefore, there was a period of 3 min and 24 s since the aircraft was stopped until the<BR>passengers were addressed. During that period, the crew had some workload to communicate<BR>with the tower, to check the status of the systems of the aircraft, to evaluate<BR>the available information that was incomplete at the first moments, and to think of<BR>the options to be followed before informing the passengers.<BR>The data retrieved in the investigation show that the air traffic control and airport services<BR>worked correctly in a coordinated manner all the time. The local air traffic controller<BR>(tower) that was controlling the traffic in runway 33 for landings kept the situation<BR>under control all the time. Runway 36R was immediately inspected and was open<BR>for traffic at 13:16 h (approximately 11 min after the aircraft came to a stop after the<BR>incident).<BR>2.5. Origin of the residual pressure<BR>The tests carried out on the aircraft and at the facilities of Messier-Bugatti led to the<BR>conclusion that the origin of the residual pressure in the left alternate brake system of<BR>the aircraft EC-IDF was the master cylinder P/N C24592020, S/N H2121 that, once disassembled<BR>from the aircraft, had a length of 170.31 mm (the nominal value was between<BR>170.050 mm and 170.100 mm) and a dead travel of 0.58 mm (the nominal value<BR>was between 0.40 mm and 0.50 mm).<BR>With those dimensions, the cylinder had to be compressed at the moment of assembly<BR>on the aircraft, in a way that made the dead travel to be 0.37 mm, which is 0.03 mm<BR>below the lowest tolerance of the specified value.<BR>45<BR>Technical report IN-062/2002<BR>In those conditions, the alternate system could work in a normal way during a lot of<BR>flights or during a lot of phases of those flights, with the only difference that the aircraft<BR>would start braking with an angle of pedal deflexion slightly below the nominal<BR>value. However, due to the thermal expansion of the hydraulic fluid during the descent<BR>from cruise, under certain conditions, it is probable that the dead travel was plugged,<BR>thus preventing the return of hydraulic fluid from chamber C1 to chamber C2 of the<BR>cylinder, and eventually building up the residual pressure.<BR>The master cylinder had passed its quality control after manufacture on 13-6-2000, and<BR>the dead travel was then measured to be 0.44 mm and the total travel 21.90 mm, with<BR>the load-travel diagram inside tolerances. The total length of the cylinder was not required<BR>to be recorded during the acceptance tests at that time. Therefore, it could not be<BR>documented whether the cylinder was already outside specifications after manufacture<BR>or whether the length of the part was unsettled later on, although it seems more probable<BR>the first possibility.<BR>The defective internal subcomponent of the cylinder that was producing the difference<BR>in actual length with respect to the nominal length, or the part of the cylinder that was<BR>ultimately responsible for the build-up of residual pressure could not be determined. No<BR>detailed analysis of the behaviour of the component was received from Messier-Bugatti.<BR>On the other hand, although Airbus carries out flight test after manufacture of their aircraft<BR>with duration of about three and a half hours, from which there are two hours at<BR>cruise altitude, and also the operator carries out acceptance flight tests, those flights did<BR>not detect any residual pressure. Since the flights did not include long periods of cruise<BR>at high altitude, it is probable that they did not produce thermal changes important<BR>enough during descent. However, the flight Tenerife-Madrid had a profile somewhat<BR>comparable to that of the flight tests (regarding time at cruise altitude) and there was<BR>indeed residual pressure.<BR>2.6. Previous history of residual pressure<BR>The aircraft was delivered by the manufacturer to the operator in May 2002. Until the<BR>date of the incident it had completed 131 flight cycles.<BR>Since 7 to 11 of June 2002 there were five abnormalities reported regarding presence<BR>of residual pressure in flight in the wheels of the left leg. In the two first cases, there<BR>was an important increase of temperature of the brakes during the landing roll.<BR>One of the squawks indicated «In descent with clean configuration the brakes residual<BR>braking lights on brake 1, 2, 5 and 6, at parking 500 °C + of temperature reached».<BR>Another report said: «In approach residual pressure in left leg brakes. Solved after seve-<BR>Technical report IN-062/2002<BR>46<BR>ral resets of nose wheel steering switch (there was indication of pressure in the brake<BR>indicator) and pressing the brakes at the same time. See previous reports».<BR>Additionally, in year 2001 there was a long history of residual pressure that affected A-<BR>340 EC-GUP of Iberia. The problem was reported to Airbus that worked with the operator<BR>to solve the problem. The TFU 32.42.21.002 stated that «Operator’s reports have<BR>shown that the ´Brakes residual braking ECAM warnings are often spurious», although<BR>it was also mentioned that they could be real and troubleshooting was needed to confirm<BR>the fault. Airbus stated that they were never formally informed of the results of the<BR>recommended trouble shooting actions of EC-GUP.<BR>Therefore, the maintenance personnel and several pilots of the operator were already<BR>familiar with the problem, and at least in one of the cases they had used several resets<BR>of the antiskid system to make disappear the pressure, although with the fundamental<BR>change of «pressing the (pedals) brakes at the same time». The deflexion of the pedal<BR>was recommended by Airbus after the incident as the way to release the residual pressure<BR>if noticed in flight (see paragraph 1.18.1). Previously, the manufacturer was not<BR>familiar with this problem, because, according to the information gathered, they had<BR>never received reports of actual residual pressure in flight from Iberia or from any other<BR>operator, and attributed any clue of pressure to spurious indications, and therefore<BR>recommended to reset the BSCU under some circumstances.<BR>Those 5 reports of abnormalities could have contributed to prevent the incident on 7-<BR>9-02 if, from an operational point of view, the information on abnormalities had been<BR>provided to the crews of A-340, it is possible that the pilots of the flight of the incident<BR>would have been familiar with the situation and with the actions taken is similar cases.<BR>Also, if from a maintenance point of view, they would have been more thoroughly<BR>investigated by the personnel of the operator, contacting with the manufacturer as<BR>needed, maybe the origin of the residual pressure would have been detected at that<BR>point. The manufacturer stated that high brake temperatures (that appeared in the<BR>first two squawks) were clear clues to indicate that the residual pressure was not<BR>spurious. Additionally, the analysis of the TSM carried out by the manufacturer showed<BR>that, with the available clues and indications, the task 32-40-00-810-927 should<BR>have been applied, at least after the third squawk according to the TSM introduction<BR>(see 1.6.5).<BR>However, it remains doubtful that the application of this task in an isolated way by the<BR>personnel of the operator would have detected the faulty component and led to the<BR>replacement of the master cylinder. The task (see 1.6.5) requests a fault confirmation<BR>by means of setting the parking brake to OFF and then looking for pressure in the triple<BR>indicator. Since the residual pressure had an intermittent nature and was no longer<BR>present after the landings in June, maybe their interpretation would have been that this<BR>«fault confirmation» action had failed and therefore the rest of the TSM task would not<BR>47<BR>Technical report IN-062/2002<BR>have been completed. Apparently they were not aware of the intermittent fault concept<BR>mentioned in the introduction of the TSM.<BR>Since the TSM has been designed to isolate/troubleshoot hard faults, it is considered<BR>that the possibility of dispatching the aircraft until having 3 intermittent occurrences of<BR>the same phenomenon should be further analysed by the manufacturer, and some additional<BR>guidance should be provided in the TSM introduction. To avoid any confusion, it<BR>should be highlighted in pertinent parts of the TSM that all available clues must be carefully<BR>considered before dispatching again an aircraft after the first and second occurrences.<BR>The operator also stated that they considered the instructions of the TFU should be<BR>applied in first place, and those instructions were not consistent with those contained<BR>in the Trouble Shooting Manual in this matter (i.e. the TFU did not refer to the proper<BR>TSM procedure). Therefore, they applied that TFU alone on the first two days of<BR>squawk.<BR>On the third day (there was no high temperature reported that day) they also checked<BR>transducers, status and condition of dual valve, master cylinder, and filter, and they performed<BR>a system test and BSCU test. The transducer, dual valve, cylinder, and filter are<BR>mentioned in the task -927 (see 1.6.5), although no task was specifically recorded on<BR>the logbook and no component was replaced.<BR>On the fourth day (with no high temperature reported) only the BSCU test and reset<BR>were carried out, which would correspond to the TFU instructions.<BR>The fifth and last day (with no high temperature reported), it seems a mixture of tasks<BR>was performed, including checking of pressure in the left leg, cleaning of transmitters,<BR>test of BSCU, and checking of wheels free to rotate. Then the squawks ceased.<BR>The operator stated, late in the investigation process, that an operational test of the<BR>brake system was carried out that day (11 June 2002), to be sure that the brake system<BR>was free of any trouble. That test is the last action of TSM task -927.<BR>The manufacturer stated that the appropriate manual to be applied is the TSM, regardless<BR>of other ad-hoc maintenance information that may have been issued. The TFU was<BR>never re-issued to match the tasks of the TSM. This TFU was closed in August 2003,<BR>once the Service Bulletins A340-32-4187 and A-340-32-4193 were issued by Airbus to<BR>solve the problem of spurious indication. It is considered convenient to issue a safety<BR>recommendation regarding the need of consistency between the different maintenance<BR>documentation.<BR>Additionally, it seemed that different interpretations existed of what to do after the<BR>«Fault confirmation» of the task 32-40-00-810-927, because the maintenance people<BR>Technical report IN-062/2002<BR>48<BR>seemed to be unaware of the intermittent failure concept of the TSM, and therefore<BR>two safety recommendations on the matter are issued.<BR>In summary, it seems that the intermittent nature of the residual pressure, together with<BR>differences of interpretation of the maintenance documentation or lack of knowledge<BR>regarding the meaning of «fault confirmation» for «hard faults» and «intermittent<BR>faults», masked the solution of the problem.<BR>The operator also stated that they used to communicate with the manufacturer in many<BR>other instances of malfunctions reported by the flight crews.<BR>The main factor that caused that the squawks in June 2002 were not communicated to<BR>Airbus was the awareness of the maintenance personnel, and even of most flight crews,<BR>of a long history of spurious cautions and indications associated to the BSCU, both in<BR>A-340 (including EC-GUP in year 2001) and in A-320, reflected in TFU and FOT of the<BR>manufacturer. Most of the corrections of the reported abnormalities included tests of<BR>the channels of the BSCU. In several instances, the correct result of those tests led to<BR>the conclusion that the caution or indication was due to a possible temporary malfunction<BR>of that component.<BR>It seems clear that this factor influenced both the line maintenance actions in Tenerife<BR>and the decisions made by the flight crew. Additionally to the history of spurious indications,<BR>there was the fact that it was a new aircraft recently delivered, and their experience<BR>indicated that in the event of an unexplained indication, the probability of that<BR>indication being spurious was greater in that period.<BR>In any case, apart from any previous history of spurious indications and from the interpretation<BR>of the available maintenance documentation, there were clues in some of the<BR>events (like high temperature after landing) to indicate that the pressure could have<BR>been real, although with an intermittent nature, and that more maintenance actions<BR>were needed.<BR>Taking into account the maintenance carried out before the incident, it was considered<BR>necessary to issue two safety recommendations regarding enhanced analysis of reported<BR>intermittent malfunctions and enhanced training to the maintenance personnel<BR>focused to analysis of reported intermittent malfunctions.<BR>After 11-6-2002, there were no further reports of residual pressure in flight until the<BR>aircraft had a bird impact on 28-7-2002 and was removed from service for repairs.<BR>Then, after the first flight since that repair, the incident happened on 7-9-2002.<BR>In summary, since 21 May (start of operation of the aircraft) until 6 June there was no<BR>report of residual pressure. Since 7 to 11 of June there were 5 reports during 5 continuous<BR>flights, and then the pressure disappeared, or at least was no longer reported,<BR>49<BR>Technical report IN-062/2002<BR>until it appeared again in the first two flights after the bird impact (Madrid-Tenerife and<BR>Tenerife-Madrid).<BR>No evidence has been found to explain this behaviour. One hypothesis was that the<BR>maintenance tasks carried out during the fixing of the 5 complaints, together with the<BR>braking during those landings, eventually «corrected» in some way the behaviour of the<BR>left master cylinder. Then, in the repairs after the bird impact, the brake pedals were<BR>disassembled and re-assembled as a whole assembly to the fuselage, and no part or<BR>subcomponent of the assembly were removed in those operations. In paragraph 1.16 it<BR>is explained that the rigging of the pedals was considered correct in the tests carried<BR>out by Airbus after the incident.<BR>In any case, it can be concluded that the tolerances and rigging of the master cylinder<BR>are so tight that, under certain conditions there may be susceptibility to environmental<BR>conditions simply by means of small deviations of those tolerances.<BR>It seems clear that it would be positive that the design of the master cylinder was modified<BR>to make it more resistant to the influence of the mentioned factors. Airbus has already<BR>initiated this and other safety actions (see 1.18.3). It is considered convenient to<BR>issue a safety recommendation related to this fact.<BR>2.7. Suitability of the operational procedures<BR>The Operations Manual of the operator did not have any procedure to be applied in the<BR>event that residual pressure was detected in flight. Neither did have the Standard Operational<BR>Procedures (SOP) of the manufacturer.<BR>When faced with this situation, a flight crew had the following options:<BR>— To take no action, with the understanding that if the Operations Manual does not<BR>say anything, there is no need to do anything, and to land in a normal way, with<BR>antiskid connected and without delaying the application of brakes. If this had been<BR>the course of action taken in the landing in Barajas, the result would have been that<BR>at touch down (should the autobrake have been connected) or at application of left<BR>brake, the residual pressure would have been released and the braking action would<BR>have been normal.<BR>— To seek technical support on the effects of the indication of residual pressure and the<BR>actions to be taken. This support could have been sought after landing in Tenerife<BR>but in flight, during the approach to Barajas and after having lowered the landing<BR>gear, it was much more complicated, because a go around would have been to be<BR>carried out to try then to communicate with the ground personnel of the operator.<BR>— To make on board the decision to initiate some action to mitigate the possible<BR>effects of that indication based in previous experience. This was the option taken by<BR>Technical report IN-062/2002<BR>50<BR>the crew in this case, using the negative experience they had in the landing in Tenerife<BR>in the same conditions of residual pressure, and therefore they decided to disconnect<BR>the antiskid and to delay the application of brakes as much as possible<BR>during the landing.<BR>After the incident, the manufacturer issued a telex to the operators (see paragraph 1.18)<BR>and modified their SOP to clarify the actions to be taken by the crew under that situation.<BR>Among those actions is to leave the antiskid connected during the landing and to<BR>press the pedals in flight to release the residual pressure.<BR>It is considered those actions are convenient to prevent similar events, because the previous<BR>SOP did not adequately cover that contingency, since an indication was described<BR>(amber bars in the page WHEEL of the ECAM) without clarifying whether it was displayed<BR>in flight, on ground or in both cases, and without providing instructions to be<BR>followed in that event.<BR>In this case, a crew faced with that situation in flight, with no information on previous<BR>similar cases and without having seen it during training, as it was this case according<BR>to the information gathered, could be unsure whether the lack of procedure was due<BR>to an omission of the manual more than to the intend of the designers that no action<BR>was needed. A more comprehensive knowledge of the brake system would have helped<BR>the crew to make the right decision. Even though the reaction of other crews of<BR>the same operator that faced residual pressure indications in flight was not the same<BR>and those flights ended with no consequences, it is considered that a more detailed<BR>study of the brake system of the A-340 during training for initial type rating would be<BR>recommendable. The manufacturer stated that their recommended syllabus was enough<BR>for the crews to understand the brake system of the A-340. The operator devoted 6 h<BR>on the ground to study the electrical, hydraulic, landing gear and APU systems. Additionally,<BR>there was a four-hour session of flight simulator to cover ECAM and failures<BR>associated to electrical and hydraulic systems.<BR>On the other hand, several discrepancies have been observed between the Operations<BR>Manual of the operator and the SOP of the manufacturer:<BR>— The manufacturer specifically recommends using the autobrake except on very long<BR>runways where it is expected that braking will not be necessary, whereas the operator<BR>says that in a dry runway of normal length, normally the use of autobrake is<BR>not necessary.<BR>— The operator requires to make a reset of the BSCU if the message «Brakes residual<BR>braking» appears on ground, while the manufacturer requires that Maintenance is<BR>advised in that case with no further action taken by the crew in the corresponding<BR>procedure of the SOP, although they allow the reset in the Chapter «Supplementary<BR>techniques». The text of the FOT of Airbus on the matter also mentions the possibility<BR>that the crew make a reset.<BR>51<BR>Technical report IN-062/2002<BR>Information retrieved from several sources indicates that there was a culture among<BR>operators that the use of the autobrake appreciably increased the worn of the brakes<BR>and also the heating (sometimes with a negative influence in the dispatch of the aircraft).<BR>Therefore, in certain occasions it was intended to limit the use of this system by<BR>crews in runways with enough length.<BR>After the incident, the operator required the use of autobrake in the procedure of the<BR>Operations Manual (2.01.63) in the event residual pressure was detected after lowering<BR>the landing gear.<BR>Although there is no requirement for the Operations Manual of an operator is completely<BR>identical to the procedures recommended by the manufacturer, in this case, given<BR>the fact that both aspects could have influenced the outcome of the incident, it is<BR>recommended that the manufacturer clarifies whether or not a reset of the BSCU should<BR>be performed on ground when the caution is displayed. The operator should then adapt<BR>their Operations Manual to the conditions established by the manufacturer in this matter<BR>and also regarding the use of autobrake.<BR>Technical report IN-062/2002<BR>52<BR>3. CONCLUSIONS<BR>3.1. Findings<BR>1. The pilots had valid licenses and were adequately qualified for the flight.<BR>2. During the descent to Madrid-Barajas Airport the residual pressure of the left brakes<BR>alternate system started increasing when the aircraft was at approximately<BR>13000 ft of altitude and it reached 800 psi when the aircraft was at approximately<BR>500 ft of radio-altitude, at 13:02:45 h.<BR>3. During the approach to Madrid-Barajas Airport, before lowering the landing gear,<BR>the crew observed in the corresponding page of the ECAM that there was residual<BR>pressure on the brakes of the left leg and, in absence of a procedure to be<BR>applied, switched off and then on the BSCU. Afterwards, they selected landing<BR>gear down and, with the gear down and locked, switched off the BSCU for 24 s<BR>and then switched it back on. They observed that there was still residual pressure<BR>on the brakes of the left leg, and disconnected again the BSCU moving the<BR>switch A/SKID & N/W STRG to the «OFF» position.<BR>4. During the landing on runway 33 of Madrid-Barajas Airport the spoilers were not<BR>armed.<BR>5. The aircraft touched down with the left and right legs of the MLG at approximately<BR>240 m past the threshold of runway 33, at 13:03:27 h. After three seconds,<BR>thrust reversers were selected, they worked normally, and the spoilers started<BR>deploying.<BR>6. The PF applied right rudder, without pressing the brake pedals, during the first 18<BR>s of the landing roll.<BR>7. Between 240 m and 900 m past the threshold of runway 33 the wheels of the<BR>left MLG burst because they were already locked when the aircraft touched down.<BR>8. At 13:03:45 h, the right brake pedal was fully deflected (68°) and the pressure of<BR>the brakes alternate system increased up to 2500 psi, when the aircraft was<BR>approximately 70 m past the intersection of runway 33 with runway 36R.<BR>9. At 73 m past that intersection there were track markings on the runway indicating<BR>that the wheels of the right leg bust in this area because they were blocked<BR>by the pressure of 2500 psi applied with the right pedal.<BR>10. The eight wheels of the left and right legs of the MLG burst because of friction<BR>with the runway surface. The tire rims 1, 2, 4, 5, and 6 showed signs of rubbing<BR>53<BR>Technical report IN-062/2002<BR>with loss of material by friction with the runway surface. The brake assemblies 1,<BR>5 and 6 showed heavy rubbing with loss of material of the casing and the disks<BR>by friction with the runway surface.<BR>11. There had been 5 complaints that referred to appearance of residual pressure in<BR>flight within 7-6-2002 and 11-6-2002 that were not notified to the manufacturer.<BR>There had also been several reports of residual pressure in other A-340 registered<BR>EC-GUP in November 2001, which had been notified to the manufacturer.<BR>12. The aircraft made on 7 September 2002 its first flight since 28 July 2002, when<BR>it had suffered a bird impact and was subject to the corresponding repair.<BR>13. The master cylinder, P/N C 24592020, S/N H2121, was the component that produced<BR>the residual pressure in flight. This cylinder had a length of 170.31 mm,<BR>which was 0.21 mm longer than specified. The dead travel of the cylinder (before<BR>being installed on the aircraft) was 0.08 mm longer than the value specified.<BR>The ultimate subcomponent inside the master cylinder that was causing the residual<BR>pressure could not be determined.<BR>14. The Operations Manual of the operator, and the Standard Operational Procedures<BR>(SOP) of the manufacturer, did not contain procedures to be followed in the<BR>event residual pressure was observed in flight. Both manuals specified that if the<BR>antiskid system was inoperative, the braking is carried out with the alternate<BR>system, and the pressure applied to the brakes must not exceed 1000 psi.<BR>3.2. Causes<BR>It is considered that the cause of this incident was the fact that, as a consequence of<BR>the appearance of residual pressure in flight in the left brakes, due to the fact that the<BR>left master cylinder P/N C 24592020, S/N H2121 was defective, and due to the lack of<BR>a procedure to be applied in that case, the crew voluntarily disconnected the antiskid<BR>system when the residual pressure was still present, which produced the burst of the<BR>left tires at touchdown.<BR>The following factors could have prevented the incident:<BR>— The existence in the Operations Manual of instructions to be followed in the case of<BR>residual pressure being observed in flight.<BR>— The knowledge by the affected flight crew of similar cases that had been reported<BR>as complaints during June 2002.<BR>— A more comprehensive analysis of the previous squawks of residual pressure.<BR>— A more detailed training on the brake system during the type rating courses.<BR>Technical report IN-062/2002<BR>54<BR>4. SAFETY RECOMMENDATIONS<BR>Airbus issued a telex to the operators in October 2002, and later on modified the<BR>FCOM to include instructions to the crew in the event of appearance of residual pressure<BR>in flight, and started a review of their procedures of checking the brake system<BR>in the assembly line of the aircraft. They also started the study of a possible modification<BR>of the design of the master cylinder to avoid the build-up of residual pressure<BR>in flight.<BR>Messier-Bugatti modified in December 2002 their procedures of quality control after<BR>manufacture of master cylinders to include the checking and recording of the total<BR>length of every cylinder. However, it could not be determined which subcomponent of<BR>the cylinder, and the environmental conditions of operation, that ultimately produced<BR>the residual pressure in flight. Therefore, it is possible that such a pressure can appear<BR>again in aircraft A-340 equipped with this type of master cylinder, and it is considered<BR>necessary to issue a safety recommendation regarding this fact.<BR>Iberia stated that they had established the «Centro de Control de Mantenimiento»<BR>(C.C.M.) with a view, among others, to improve the communication with remote maintenance<BR>units.<BR>REC 09/04. It is recommended to the DGAC of France that, in collaboration with Airbus<BR>and Messier-Bugatti, conducts a deep evaluation of the characteristics<BR>of design, manufacture and maintenance of the master cylinders of<BR>the brake system of the A-340. This evaluation should have the goal of<BR>preventing that cylinders accepted by the different quality controls of the<BR>manufacturers at component manufacturer, final assembly, and flight testing,<BR>might produce residual pressure on the brake system under certain<BR>conditions of operation.<BR>REC 10/04. It is recommended to the DGAC of Spain to encourage Iberia to take<BR>action to improve the communication channels between their different<BR>departments in a way that allows that flight crews and maintenance personnel<BR>may, at any time and from any airport, seek quick and effective<BR>engineering and operational support regarding situations not adequately<BR>covered by the manuals available to them.<BR>REC 11/04. It is recommended to the DGAC of Spain to encourage Iberia to improve<BR>their methods of analysis of reports of abnormalities by the flight crews,<BR>consulting with the manufacturer when needed, in such a way that it is<BR>prevented the intermittent appearance of the same complaint, and that<BR>the useful information resulting from that analysis is provided to flight<BR>crews and maintenance personnel.<BR>55<BR>Technical report IN-062/2002<BR>REC 12/04. It is recommended to the DGAC of Spain that the training methods provided<BR>to the applicable maintenance personnel of Iberia are monitored in<BR>order to assure that in the correction of the reports of intermittent malfunctions<BR>provided by flight crews, all the available maintenance documentation,<BR>as well as all the available clues, are used to analyse the causes<BR>of the malfunctions.<BR>REC 13/04. It is recommended to Airbus that they should revise the content of the<BR>pertinent parts of the TSM in order to provide additional guidance regarding<BR>the maintenance procedures to be applied in the event of intermittent<BR>faults, taking into account the kind of fault and the available clues<BR>before dispatching again the aircraft. All operators should be informed on<BR>the results of that revision.<BR>REC 14/04. It is recommended to Airbus that in the training they provide to maintenance<BR>personnel there is enough information to deal with intermittent failures.<BR>REC 15/04. It is recommended to Airbus that it should be assured that the TSM and<BR>other specific or temporary maintenance documentation, like a «Technical<BR>Follow-up», is consistent and equally updated in regard to their technical<BR>content.<BR>REC 16/04. It is recommended to the DGAC-France that the training syllabus recommended<BR>by Airbus to the airlines for type rating of A-340 is reviewed in<BR>order to assure that it leads to an adequate understanding of the details<BR>of the brake system of the aircraft.<BR>REC 17/04. It is recommended to the DGAC-Spain that the training syllabus used by<BR>Iberia for initial type rating of flight crews in Airbus A-340 is reviewed to<BR>assure that enough time is devoted to reach an adequate understanding<BR>of the details of the aircraft brake system. This review should take into<BR>account any possible change in the Airbus recommended syllabus.<BR>REC 18/04. It is recommended to Airbus that the content of the Abnormal Procedures<BR>and Supplementary Techniques of the A-340 FCOM are revised to<BR>unify the criteria of actions to be taken when the caution «Brakes residual<BR>braking» is displayed on ground.<BR>REC 19/04. It is recommended to Iberia that their Operations Manual of the A-340 is<BR>updated with the guidelines provided by Airbus regarding the use of<BR>autobrake during landing and the actions to be taken when the caution<BR>«Brakes residual braking» is displayed on ground.<BR>Technical report IN-062/2002<BR>56<BR>57<BR>Technical report IN-062/2002<BR>APPENDICES<BR>59<BR>Technical report IN-062/2002<BR>APPENDIX A<BR>Diagram of tracks on runway 33<BR>of Madrid-Barajas Airport<BR>61<BR>Technical report IN-062/2002<BR>Technical report IN-062/2002<BR>62<BR>63<BR>Technical report IN-062/2002<BR>APPENDIX B<BR>Details of the trouble shooting procedure<BR>applied after the incident<BR>(1 TO 4 ARE ITEMS TO PREPARE THE AIRCRAFT FOR THE PROCEDURE)<BR>...<BR>5. Check for pressure (LH & RH ALT brake) using the cockpit triple gauge.<BR>If pressure remains, Go to (6)<BR>If no pressure remains, Go to (8).<BR>6. If RH ALT pressure, unscrew caps K on the BDDV (5403GG)<BR>If LH ALT pressure, unscrew cap I on the BDDV (5403GG)<BR>If the pressure remains on the triple gauge, replace the BDDV (5403GG)<BR>If the pressure clears on the triple gauge, replace LH (5422GG) or RH (5423GG) master<BR>cylinders.<BR>7. Repeat tests (5) & (6).<BR>If the pressure remains, the Dual Shuttle Valve (5404GG) should be replaced.<BR>If the pressure clears, a dimension check of brake pedal rigging is required.<BR>A quick test is to measure the distance between centre lines of master cylinder mounting<BR>holes. They should be the same as each other and be within the range of<BR>170+0.1/+0.05mm.<BR>Note that no compression of the Master Cylinder should be required to mount it in position.<BR>(Further checks see AMM 32-43-12-000-801, Removal of the Cockpit Alternate<BR>Brake Master Cylinders).<BR>8. Fully depress and then release LH & RH brake pedals.<BR>If pressure remains on pedal release, Go to (6).<BR>If pressure clears on pedal release, Go to (9).<BR>9. Apply and release park brake.<BR>If the pressure remains, the Dual Shuttle Valve (5404GG) should be replaced and test<BR>repeated. (AMM 32-43-14-400-801 Dual Shuttle Valve – Removal/Installation).<BR>If the pressure clears on parking brake release, go to (10).<BR>10. If residual braking cannot be reintroduced, the following modified low-pressure<BR>circuit bleeding procedure (AMM 32-43-00-870-801, replenishment of the Alternate<BR>Braking Control Reservoir) should be used to check for restrictions in the low-pressure<BR>circuit.<BR>65<BR>Technical report IN-062/2002<BR>With all AIC systems depressurised, attach a bleed hose to the bleed valve of the alternate<BR>brake control reservoir (5424GG). Put the other end in a container to catch the<BR>fluid. Drain until no fluid flows.<BR>Unscrew cap a port ‘J’ of the BDDV and attach a bleed adapter (as identified in the bleeding<BR>procedure). Measure the flow to the bleed container from port ‘J’ of the BDDV<BR>(5403GG) when supplying fluid at a pressure of up to 4 Bars.<BR>NOTE: Once the bleed valve opening is set for the first the test on side J (WH side) it<BR>should remain in the same position for side K (RM side).<BR>The supply flow and pressure set for the first the test on side J (L/H side) should remain<BR>in the same position for side K (RIH side).<BR>Repeat the above, this time connecting the port K of BDDV (5403GG).<BR>Compare the flow rate from the pipe into the container. If the flow rates from the two<BR>sides are different or are restricted, a blockage is suspected.<BR>11. Detach the master cylinder with restricted flow from the pedal assembly. Carry out<BR>a flow rate check as in (10).<BR>If flow rate does not increase to rate of the ‘good’ side, then the master cylinder should<BR>be replaced.<BR>If flow rate increases to rate of the ‘good’ side, then the pedal assembly should be<BR>removed and re-rigged.<BR>END OF THE PROCEDURE<BR>Technical report IN-062/2002<BR>66 学习了!:)
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