Acoustic Panel Delamination
**** Hidden Message ***** February 2002 WTT face to face CFMI / Boeing Proprietary Information - Unauthorized Disclosure, Use, or Export are Prohibited 1<BR>Acoustic Panel Delamination<BR>February 2002 WTT face to face CFMI / Boeing Proprietary Information - Unauthorized Disclosure, Use, or Export are Prohibited 2<BR>CFM56-7B IDG Acoustic Panel Rupture<BR>Background<BR>• Several cases of IDG panel failure on CFM56-7B Engines reported<BR>• Failure discovered with lowest operational time at 1,500 hrs / 500 cycles<BR>Acoustic Panel Delamination<BR>February 2002 WTT face to face CFMI / Boeing Proprietary Information - Unauthorized Disclosure, Use, or Export are Prohibited 3<BR>Investigation status<BR>• Mechanical potting characteristics decrease through temperature and aging<BR>phenomenon<BR>• Cracks beginning in the Honeycomb following by cut out of the outer skin then<BR>tearing of the inner skin layer<BR>• Phenomenon generated by vibratory excitation<BR>CFM Recommendation<BR>• Panel to be removed when found cracked<BR>• 500 cycles Service Extension allowed with panel removed (AMM72-23-02<BR>Jun, 2001)<BR>CFM56-7B IDG Acoustic Panel Rupture<BR>Acoustic Panel Delamination<BR>February 2002 WTT face to face CFMI / Boeing Proprietary Information - Unauthorized Disclosure, Use, or Export are Prohibited 4<BR>Corrective Actions<BR>• Design improvement<BR> Upper and inner skins material changed to increase temperature<BR>characteristics : From 120°C to 180°C<BR> Panel Potting change for better behavior in high temperature<BR>environment conditions : From Minnesota to E3439<BR> Manufacturing process changed to increase hole edge strength<BR> Design finalized, to be approved by Agencies Apr 02<BR> Implementation in production Jul 02<BR>CFM56-7B IDG Acoustic Panel Rupture<BR>Acoustic Panel Delamination :victory: :victory: Acoustic Panel Delamination
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