航空 发表于 2011-4-15 08:59:01

CFM 737 N1/N2 Vibration Team Report

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航空 发表于 2011-4-15 08:59:13

1<BR>Boeing and CFMI February 5, 2002 Proprietary Information<BR>737 N1/N2 Vibration Team Report<BR>2<BR>Boeing and CFMI February 5, 2002 Proprietary Information<BR>737 / CFM56-7B N1 Vibration / N2 Tone<BR>• The current aircraft / engine vibration related noise / vibration<BR>levels do not consistently meet customer expectations without<BR>significant flight line disruptions<BR>• Define / implement solutions with goal of B1/C1<BR>• No quality impact<BR>Problem Statement<BR>Boeing / CFMI Team Charter<BR>N1/N2 – 3P Team Status<BR>3<BR>Boeing and CFMI February 5, 2002 Proprietary Information<BR>N2 Tone - 2001<BR>• Ground Tone<BR>• Not a major flight line cause disruption<BR>• Can result in engine removals<BR>• In-Flight Tone<BR>• Not a problem since 10/99 S/W mod<BR>• Slight increase squawk activity in summer 2001<BR>0<BR>10<BR>20<BR>30<BR>40<BR>50<BR>60<BR>70<BR>80<BR>J a n<BR>M a r<BR>M a y<BR>J u l<BR>S e p<BR>N o v<BR>J a n<BR>M a r<BR>M a y<BR>J u l<BR>S e p<BR>N o v<BR>Month<BR>E n g in e S q u a w k R a t e - %<BR>RTV Buttons<BR>Squawk Rate<BR>Repeat Squawk Rate<BR>Flight Line N1 Vibe - 2001<BR>Flight Line N1 Vibe Squawk Rates<BR>•Major flight line disruption cause<BR>• Low N1 vibe levels required to support delivery<BR>• Challenging VENOS (interior noise/vibe) delivery criteria<BR>• RTV/ Buttons have improved situation<BR>• Squawk / repeat squawk rates still unacceptable<BR>• AVM Solution / Fan Trim typically resolves squawks<BR>• Repeat squawks result in retrim, fan blade relube or<BR>engine removal<BR>Engine Vibe Related Squawk Distribution<BR>June to Sept 2001<BR>7%<BR>13%<BR>77%<BR>3%<BR>N1 AVM&gt; 1.0<BR>N1 AVM &gt; 1.0 &amp;<BR>A&amp;T<BR>N1 A&amp;T<BR>N2<BR>N1 A&amp;T Major<BR>Cause of Squawks<BR>2000 2001<BR>N1/N2 – 3P Team Status<BR>4<BR>Boeing and CFMI February 5, 2002 Proprietary Information<BR>Purpose:<BR>• -599 /Airplane Inst’l Effects<BR>• Optimized Balance Process<BR>• Determine Aircraft/Engine sensitivity to unbalance<BR>• Airplane Loading Impact / Flight maneuver effects<BR>Key Findings:<BR>• LPT unbalance verified / correct w/ 2-Plane trim<BR>• Quantified sensitivity to Fan/LPT unbalance<BR>• TRF sensor is better indicator of LPT unbalance than FFCC<BR>• Impact of fuel and airplane loading measured<BR>Production A/P Flt Test<BR>Eng -599 on YA106<BR>Strut Shake Test<BR>YA106 ‘GVT’<BR>Purpose:<BR>• Data to Develop Math Model for<BR>Airplane A&amp;T prediction<BR>• Use to identify and evaluate fixes<BR>Key Findings:<BR>• Strut structure resonances found in<BR>N1and N2 ranges<BR>Eng -599<BR>Investigation at CFMI Test Cell<BR>Purpose:<BR>• Compare Fan/LPT unbalance vs On-wing<BR>• Investigate LPT unbalance source<BR>• Quantify improvement to #5 ODB mod<BR>Key Findings:<BR>• Balance solution test cell vs. on-wing similar<BR>• High LPT unbalance confirmed<BR>• Not typical of current manufacturing process<BR>• Process change implemented to prevent reoccurrence<BR>• #5ODB testing scheduled Feb-Mar 20002<BR>Solution Development Test<BR>YA106 (phase 2)<BR>Purpose:<BR>• FCSB / Fairing / Strut Transmissibility Test<BR>• Local N1 Treatment and Passenger Load Testing<BR>Key Findings:<BR>• Fuel loading has significant impact<BR>• N1 Tone reduction FCSB possible – testing TBD<BR>• Proposed N1 treatment not effective<BR>• Investigating new configuration<BR>N1/N2 – 3P Team Status<BR>5<BR>Boeing and CFMI February 5, 2002 Proprietary Information<BR>3D MWFan Blades<BR>• Proceeding with immediate implementation of<BR>the following three solutions<BR>• 2 Plane Trim Balance (CFMI test cell)<BR>• 3D MW Fan Blades (CFMI new production)<BR>• Improved AVM Balance Algorithm (New A/Ps)<BR>• Assess flight line benefit for<BR>• N1 AVM, N1 Audible, N1 Tactile<BR>2 Plane Trim Balance (LPT Balance) Improved AVM Balance Algorithm<BR>• Currently fan blades mapped for radial moment weight (MW)<BR>only<BR>• New procedure allows blades to be mapped for radial,<BR>tangential, and axial fan blade MW at new engine delivery<BR>• Results in fan blade sets with lower fan unbalance<BR>- Expect improvement in ability to trim balance engine to<BR>achieve lower vibe levels consistently<BR>- Minor improvements in N1 AVM and A&amp;T<BR>• Intro at CFMI test cell Jan 2002<BR>• No field impact regarding fan blades &amp; procedures<BR>• Fan trim balance performed to reduce N1 engine vibe<BR>levels and N1 A&amp;T<BR>• Currently assessing benefit of 2 plane trim balance<BR>for N1 A&amp;T levels and flight line disruption rate<BR>• 2 plane trimmed (as req’d) at CFMI starting 888-769<BR>• Flight line evaluation in progress<BR>• Go-Forward plans - April, 2002<BR>• CFMI All OPS Wire issued Dec 2001<BR>• S/B 72-0347R1 introduced LPT Stage 4 clips<BR>• Procedure not intended for in-service use<BR>• Improve quality of data collected for fan trim solutions<BR>• Speed ranges<BR>• Stability requirements<BR>• Coefficients<BR>• Reduce A/P noise and vibration and AVM levels<BR>•Improved ability to resolve squawks at &gt;95% N1<BR>• Available on production AVM units Q2 2002<BR>• Retrofit not required, but available<BR>Category 1 Solutions<BR>N1/N2 – 3P Team Status<BR>6<BR>Boeing and CFMI February 5, 2002 Proprietary Information<BR>Other Solutions Being Considered<BR>• #5R Oil Damped Bearing Optimization<BR>• Local Airplane Treatment for N1<BR>• Fan Blade Break-in<BR>• Optimized Fan Cowl Support Beam<BR>• #3R Bearing Clearance<BR>• Optimized Interior Modification for N2 tone<BR>• AVM and VENOS Measurement and Criteria<BR>• Active Vibration Control<BR>N1/N2 – 3P Team Status<BR>7<BR>Boeing and CFMI February 5, 2002 Proprietary Information<BR>Summary<BR>• Engine related N1 / N2 vibes are major flight line disruption cause<BR>• Boeing / CFMI team charted to implement solutions to achieve B1 / C1 goal<BR>• No quality impact<BR>• Category 1 solutions being implemented / evaluated - 1Q2002<BR>• No in-service impact<BR>• Other potential solutions being considered - 4Q2002<BR>N1/N2 – 3P Team Status

kinran 发表于 2011-6-4 23:24:38

:victory: :victory:

bocome 发表于 2011-7-31 04:45:43

CFM 737 N1/N2 Vibration Team Report

bei1999 发表于 2016-5-3 06:09:48

737-800中文AMM手册
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