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B737-Center_Tank_Fuel_Pumps中央邮箱燃油泵 [复制链接]

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1#
发表于 2010-4-5 01:20:09 |只看该作者 |倒序浏览

B737-Center_Tank_Fuel_Pumps中央邮箱燃油泵

 

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2#
发表于 2010-4-5 01:20:36 |只看该作者
737.1
Center Tank Fuel Pumps
Terry Sheehan
737NG Procedures Manager
Boeing Commercial Airplanes
May 2004
The Boeing Company 737.2
Hydro-Aire Fuel Pumps
• Two areas of concern were identified on Hydro-Aire
fuel pumps installed on 737-600/-700/-800/-900
airplanes
– Wire chafing
– Localized overheating
• Two separate Airworthiness Directives issued
– Both mandated similar operational restrictions
Baacckkggrroouunndd
The Boeing Company 737.3
Background
• In August 2002, teardown of several failed Hydro-
Aire fuel pumps indicated the potential existed for
wires to come in contact with the rotor as a result of
installation errors
• Evidence of arcing due to chafed wires was
discovered
Wiirree Chhaaffiinngg
The Boeing Company 737.4
Background
Wiirree Chhaaffiinngg
The Boeing Company 737.5
Background
Wiirree Chhaaffiinngg
The Boeing Company 737.6
Background
• In response, the FAA released AD 2002-19-52
which mandated operational restrictions
• The AD provided terminating action
– Inspection of pumps per Boeing or Hydro-Aire
Service Bulletin required prior to installation
– Once center tank fuel pumps inspected and
found to be in compliance, the operational
restrictions could be removed on an airplaneby-
airplane basis
Wiirree Chhaaffiinngg
The Boeing Company 737.7
Background
• In October 2002, evidence of extreme localized
overheating in the area of the primer impeller was
found on several in-service fuel pumps
• Further investigations indicated the potential for
extreme over-temperature exposure outside the
explosion proof chamber of the fuel pump existed
Looccaalliizzeedd Ovveerrhheeaattiinngg
The Boeing Company 737.8
Background
Looccaalliizzeedd Ovveerrhheeaattiinngg
The Boeing Company 737.9
Background
Looccaalliizzeedd Ovveerrhheeaattiinngg
The Boeing Company 737.10
Background
• The FAA released AD 2002-24-51 which reinstated
the requirement to maintain minimum fuel levels to
keep center fuel tank pump inlets covered
• No terminating action defined
Looccaalliizzeedd Ovveerrhheeaattiinngg
The Boeing Company 737.11
Background
• In June 2003, the FAA issued Approval Letter
140S-03-189 to allow a “staged shutoff” following
approved X-ray inspection of center tank fuel
pumps
– Allows all fuel in the center tank to be used
• A Flight Crew Operations Manual Bulletin was
released to provide operating instructions
– Either the AD procedures or the AMOC
procedures to be used at the discretion of the
airline
Alltteerrnnaattiivvee Meetthhoodd ooff Coompplliiaannccee ((AMOC))
The Boeing Company 737.12
Design Improvements
• Original Master Caution system logic requires both
center tank fuel pumps to indicate low pressure
before the Master Caution and FUEL annunciation
illuminate
• With the new system logic, a low pressure condition
for either center tank fuel pump will illuminate the
Master Caution and FUEL annunciation
Maasstteerr Caauuttiioonn SSyysstteem
The Boeing Company 737.13
Design Improvements
• A center tank fuel pump is automatically shut off
after approximately 15 seconds of continuous low
pressure
– No indication to the flight crew
• Considered a backup to normal flight crew actions
• If fuel remains in the center tank, the system can be
reset by turning the fuel pump switch OFF, then ON
Auuttoomaattiicc SShhuuttooffff
The Boeing Company 737.14
Design Improvements
• In the original design, the alert is displayed if the
center fuel tank contains more than 1600
pounds/726 kilograms of fuel and both center tank
pumps are producing low or no pressure
• In the new design, the alert will be displayed if the
center tank contains more than 1600 pounds/726
kilograms of fuel and both center tank pumps are
OFF
CONFIIG Alleerrtt
The Boeing Company 737.15
Revised Normal Procedures
The Boeing Company 737.16
FAA Action
• Boeing has proposed the Master Caution system
logic change and center tank fuel pump automatic
shutoff feature as terminating action for AD 2002-
24-51
• Boeing believes the FAA will mandate these
changes and propose a 36-month compliance time
after release of the Service Bulletin
• FAA decision is imminent
The Boeing Company 737.17
Design Improvements
• All three design changes will be available in
production in May 2004 (Line Number 1494 and on)
• Available via Service Bulletin in 4th Qtr 2004
Avvaaiillaabbiilliittyy –– 773377 NG
The Boeing Company 737.18
Design Improvements
• Master Caution system logic change will be
available via Service Bulletin in 4th Qtr 2004
• Automatic shutoff feature will be available via
Service Bulletin in 3th Qtr 2005
Avvaaiillaabbiilliittyy –– 773377--220000 tthhrroouugghh --550000
The Boeing Company 737.19
Design Improvements
• Wire retention system
– Prevents wires from contacting rotor due to
installation errors
– Scheduled to be available in 2nd Qtr 2005
– Boeing is proposing this change as terminating
action for AD 2002-19-52
• Replacement fuel pump
– Scheduled to be available in 24 to 36 months
Fuuttuurree Deessiiggnn Feeaattuurreess

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3#
发表于 2010-6-11 00:29:18 |只看该作者

回复 1# 民航 的帖子

先顶后下!!!!!!!!

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4#
发表于 2010-6-12 07:41:47 |只看该作者
看看看,谢谢楼主

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5#
发表于 2010-11-10 08:48:48 |只看该作者
看看看,谢谢楼主

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6#
发表于 2010-11-17 11:25:39 |只看该作者
顶顶看什么好东西

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7#
发表于 2011-1-6 22:04:49 |只看该作者
先顶后下!!!!!!!!

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8#
发表于 2011-1-7 12:13:05 |只看该作者
sdfsfdsfsfsddfs

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9#
发表于 2011-1-9 10:26:43 |只看该作者
多谢分享啊

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10#
发表于 2011-1-19 22:28:11 |只看该作者

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